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Latest Experiment…Failure!

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Old 04-13-11, 05:07 PM
  #276  
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Originally Posted by Barry Bordes
As an update the "failure".... it is still running 3 years later. I do have to re-Loctite the spark plug at each replacement.

The latest experiment is with the in-chamber sensor where we just broke 1000 psi chamber pressure for the first time (10 lb wastegate spring goes to 12psi).



Barry I've been in discussion with another forum member as to the potential combustion pressures inside the rotary during a water steam clean. Would you be interested in performing such a test?
Old 04-14-11, 09:07 PM
  #277  
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Originally Posted by t-von
Barry I've been in discussion with another forum member as to the potential combustion pressures inside the rotary during a water steam clean. Would you be interested in performing such a test?
He currently is running around 5-600ccs of 50/50 water/meth, so what you are seeing is a 10-12psi pull on water/meth.

-J
Old 04-15-11, 07:53 AM
  #278  
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Quote:
Originally Posted by t-von
Barry I've been in discussion with another forum member as to the potential combustion pressures inside the rotary during a water steam clean. Would you be interested in performing such a test?


Originally Posted by Gorilla RE
He currently is running around 5-600ccs of 50/50 water/meth, so what you are seeing is a 10-12psi pull on water/meth.

-J
And t-von, I am a little afraid to turn off the water! But what test do you suggest?

So far we have looked at advanced timing and split.

Barry
Old 04-15-11, 03:45 PM
  #279  
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Usually "steam cleans" are done in neutral with no load, just free reving...

But if that is what he is talking about, then the ICP will be quite low.

-J
Old 01-02-12, 07:04 AM
  #280  
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A little update with pictures.

The main reason for the housing bump (and subsequent breaking or warping of apex seals) is the problem of high spark plug temps.
Ironically the problem was worsened by an "improvement" to the later production engines.
Understanding this leads to a solution (or a least the method to mitigate the temps).

Mazda publishes very accurate diagrams. This one shows a 13B improvement of moving the leading plug further from the trailing to help increase burn-rate.
Unfortunately this decreases the size of the most critical water passage in the engine (see yellow arrow).

Back to the solution. All we have to do is recreate Mazda's original size passage without getting any closer to the plug casting area.

Barry


Old 01-02-12, 01:32 PM
  #281  
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i was too lazy to go find it again, but there is a photo gallery somewhere of this http://www.youtube.com/watch?v=mzJGFBJlJrc

i'd suggest you copy THOSE, as that engine without the restrictor is making substantial HP on pump gas, and it goes a long time between rebuilds. it gets a lot of miles too, i've seen it run at laguna almost every year since 2001...

i dig the 4 rotor seal case
Old 01-03-12, 01:27 PM
  #282  
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Man-o-man, Do I feel slow. I have half the number of parts and those guys build the 4 rotor in thirty seconds.

I wonder if those housings are cut at the through bolts and only supported by the plug bosses?

Barry

Originally Posted by j9fd3s
i was too lazy to go find it again, but there is a photo gallery somewhere of this http://www.youtube.com/watch?v=mzJGFBJlJrc

i'd suggest you copy THOSE, as that engine without the restrictor is making substantial HP on pump gas, and it goes a long time between rebuilds. it gets a lot of miles too, i've seen it run at laguna almost every year since 2001...

i dig the 4 rotor seal case
Old 01-03-12, 05:00 PM
  #283  
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from http://www.autoblog.com/2011/05/20/m...anniversary-o/

i swear there was a pic where you can see the reliefs, but i can't find it, maybe you have to pause the video?
Old 01-07-12, 04:48 AM
  #284  
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I'm going to give this a go and see if it helps cure the leading plug high spot. I hope to make 600rwhp on pump gas initially, then ultimately 700rwhp, probably on E85.
Also, I enlarged the gallery below the leading plug as barry mentioned.
Attached Thumbnails -photo-.jpg  
Old 01-10-12, 09:59 AM
  #285  
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Me and my engine builder are going to use some of these ideas on a p-port turbo motor we're building. We really like the idea of running cooling lines to the rear plugs coming off the water pump. Only thing is that it makes more sense to run two individual lines instead of teeing off one line.

Also, if eliminating boiling at the rear leading plug is one of the objectives I'm surprised no one has brought up Evans NPG coolant. Evans has a boiling point of 380F and should eliminate the problem of boiling at the rear leading plug.

I think everyone is coming up with some great ideas here and I hope others can contribute more to solving this coolant problem. Here are some pictures of the coolant lines me and my engine builder ran to the rear plugs.

-4m3xwl.jpg
-yavrql.jpg
Old 01-10-12, 12:22 PM
  #286  
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Also, if eliminating boiling at the rear leading plug is one of the objectives I'm surprised no one has brought up Evans NPG coolant. Evans has a boiling point of 380F and should eliminate the problem of boiling at the rear leading plug.


I did on page 1


I run Evans NPG+ in a zero pressure system and it really helps eliminate minor leaks and its properties should alleviate the problems of lack of heat transfer at the plugs due to vapor barrier.


Like you, I believe the cooling problem being addressed here is caused by a localized hot spot that exceeds the vapor pressure of the coolant used and the resulting vapor deposition on the rotor housing walls inhibits heat transfer.

However, some tracks only allow water in the cooling system as a safety measure.
Old 02-02-12, 02:07 PM
  #287  
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So you just drilled and tapped next to the plugs?

Originally Posted by Ball joint
Me and my engine builder are going to use some of these ideas on a p-port turbo motor we're building. We really like the idea of running cooling lines to the rear plugs coming off the water pump. Only thing is that it makes more sense to run two individual lines instead of teeing off one line.

Also, if eliminating boiling at the rear leading plug is one of the objectives I'm surprised no one has brought up Evans NPG coolant. Evans has a boiling point of 380F and should eliminate the problem of boiling at the rear leading plug.

I think everyone is coming up with some great ideas here and I hope others can contribute more to solving this coolant problem. Here are some pictures of the coolant lines me and my engine builder ran to the rear plugs.


Old 02-08-12, 09:32 AM
  #288  
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Originally Posted by RexRyder
So you just drilled and tapped next to the plugs?
Yes, you actually drill into the metal that divides the two coolant jackets above and below the plug.
Old 02-08-12, 09:56 AM
  #289  
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^Are those steel NPT fittings threaded into the aluminum housings?
Old 02-08-12, 11:00 AM
  #290  
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Originally Posted by BLUE TII
[I]
However, some tracks only allow water in the cooling system as a safety measure.
coolant is very slippery! [band camp] this one time i was behind a new turbo porsche on the track, and it blew a hose off, and as soon as stuff hit the windshield the car was sideways, in a straight away [/band camp]
Old 02-08-12, 01:28 PM
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Originally Posted by Trots*88TII-AE*
^Are those steel NPT fittings threaded into the aluminum housings?
Yes

This is a drag motor which consequently won't see that much run time. Because of this I'm not worried about corrosion. That and there is a ton of pipe dope and Teflon tape acting as a barrier.
Old 02-08-12, 02:00 PM
  #292  
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Originally Posted by Ball joint
Yes

This is a drag motor which consequently won't see that much run time. Because of this I'm not worried about corrosion. That and there is a ton of pipe dope and Teflon tape acting as a barrier.
Cool, I'm not going to speculate or tell you how to build your stuff, I just would have thought the different expansion rates could cause leaks or put stress on the area (just like fittings in the front iron oil feed), but I could very well be wrong. I'm thinking of doing a similar thing, but with straight aluminum threads & o-rings and then tacking them to the housing.

I forgot how much I liked this thread, what's new Barry?
Old 03-05-12, 09:13 PM
  #293  
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Old 05-12-13, 02:17 PM
  #294  
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Anything new???
Old 05-12-13, 04:10 PM
  #295  
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Originally Posted by Ball joint
Yes

This is a drag motor which consequently won't see that much run time. Because of this I'm not worried about corrosion.
And then there's all of the other steel things threaded into aluminum... we generally call them bolts and studs

People don't freak out about putting special goops on bolts when they put their intake manifolds together or such, do they?
Old 06-13-13, 10:50 PM
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Old 05-13-14, 03:00 PM
  #297  
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I'm bumping this...


So, after reading through everything and seeing similar things done over the years, what would be the best combination to keeping heat out of the "hump" in the spark plug area?

I'm building a turbo Renesis and I have been debating on drilling and tapping the area around the spark plugs and running coolant lines like a few others have. I'm just curious to know if some long term results are in since this is an older thread.

Also, I been looking at the Renesis irons and trying to figure a way to do something similar near the exhaust port since this is a failure point on turbo Renesis motors just as the spark plug area on all other 12a and 13bs.
Old 05-13-14, 09:54 PM
  #298  
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And I'm going to reply. I am not a rotary racer or expert but I'm looking at this problem and thinking, as the machinist I am. I look as this picture and hear the conversation about cutting through the ribs.



Why just cut through the rib? Once compromised, just remove the whole thing. Then add a bridge. One could go as simple as using a Bridgeport type machine (or a lessor, even bench top Chinese cheapy) and plunge a say... 1/4" endmill into the meat of the walls, precision located by the dials or a DRO, dirctly opposite each other, basically producing a half moon shape. Then making a simple insert from 1/4" stock, radiused properly on the ends, that has a slight press fit, tapping it in, and then flushing it to the housing.

You could even knife edge the ends after install.
Attached Thumbnails -photo-.jpg  

Last edited by TonyD89; 05-13-14 at 09:58 PM.
Old 05-14-14, 04:30 AM
  #299  
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That pic looks really small on my pc, any chance you can upload it so it is full size?

The idea behind cutting the ribs I think is that as the piece where the spark plug is screwed heat up and expands, the ribs do do not heat up and pull on the inner envelope where the spark plug boss expands and makes the inner envelope no plane anymore, causing the known loss of sealing everywhere apart from around the leading plug.

when the ribs are cut, they cannot pull on the inner envelope and this way as the spark plug boss heat up and pushes the chrone imwards, it will move over the entire width inwards and not just on the around the leading hole, thus maintaining a more straight sealing surface.

at least thats what I tought how it worked..
Old 05-14-14, 10:45 AM
  #300  
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As an update. I had previously ported the passages shown around the lower plug (yellow arrow).

After 50k miles I removed the motor to find no hump carbon stains!

So you don't need supplemental tubes to maintain the temps around the plug.

Barry

Originally Posted by Barry Bordes
A little update with pictures.

The main reason for the housing bump (and subsequent breaking or warping of apex seals) is the problem of high spark plug temps.
Ironically the problem was worsened by an "improvement" to the later production engines.
Understanding this leads to a solution (or a least the method to mitigate the temps).

Mazda publishes very accurate diagrams. This one shows a 13B improvement of moving the leading plug further from the trailing to help increase burn-rate.
Unfortunately this decreases the size of the most critical water passage in the engine (see yellow arrow).

Back to the solution. All we have to do is recreate Mazda's original size passage without getting any closer to the plug casting area.

Barry




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