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Replaced TB= ran good then bad

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Old 05-23-04, 11:31 PM
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Replaced TB= ran good then bad

Ive got a really wierd setup guys.. Im running a TII block with the TII intake manifolds and NA exhaust. So obviously I do not have a turbo. I am using teh s4 NA harness and ECU. Now that you know my setup read about my problem please.

I had the NA TB on there at first, then I found out I can just use teh TII TB and have everything more accesable. I put that on today, but since the TPS on there is s5 and the s4 TPS will not bolt up on this TB I had to do a little splicing. I left the s5 TPS on the TB, but spliced in the s4 connector to the same color wires. I started up the car and wow it started up so fast, better than ever before. I fine tuned it a little and it ran so good, idle was very smoooth and revved up very fast. I took it for a drive and wow it felt like it had way more power. The car just took off. I got to the end of my street and this happend:

I let go of the throttle and the idle starts bouncing up and down from 1.5k to 2k. So I jump up pop the hood and disconnect the TPS thinking its the problem. With the TPS disconnected the idle just shot up to 4k and stayed there.

If you have any idea of what the problme is PLEASE tell me. I really need to get her running good so I can commute.
Old 05-24-04, 11:51 AM
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bump
Old 05-24-04, 12:10 PM
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Sounds like a big vac leak..
Maybe in the AWS circuit?
Old 05-24-04, 08:25 PM
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the TB mod is done on it, so no AWS
Old 05-24-04, 08:46 PM
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What method did you use to fill the holes on the tb?
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