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Blew the motor on the dyno getting ready for Summer Slam!

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Old 06-21-09, 02:24 PM
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Blew the motor on the dyno getting ready for Summer Slam!

Bad News - blew the motor Sat morning on the dyno

Good news - car is back up and running Sat night and will be ready for Summer Slam.

This is the short version, I'll update the rest in a few.

Before it blew it made 603 HP at 30 psi on E85 and methanol with air fuels in the low 10's with NGK 10.5 Race plugs.

Anthony

Last edited by ErnieT; 02-04-10 at 02:38 AM. Reason: At request of poster
Old 06-21-09, 02:27 PM
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Sorry to hear man, what was the cause?

Sounds like it would have made some good power with the afr's lined out.
Old 06-21-09, 02:47 PM
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whats the specs on the new motor oR did you guys just Fix the broken items
Old 06-21-09, 04:55 PM
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glad to hear your back up and running.
Old 06-21-09, 07:31 PM
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I had the re-tune the because I added 2 additional 1680cc injectors for the E85. I started off on wastegate spring (17psi on my car) and made 465 with air fuels in the low 10's. I then turned on the meth injection and had to lean it out a lot (over 20%) and it made the same power. I just wanted to compare.

Now I turned up the boost to 30 psi. First pass it made just over 600 with the air fuels in the low 10's. It was a clean pass, intake temps were good, coolant temps were perfect and air fuels were perfect. 2nd pass was also perfect, made the same power. I let it cool down and wanted to run 35psi. On that pass the motor blew going into the power band. Boost did not get past 30 (same issue with this boost controller) and it was on point to making a clean pass, air fuels from the datalog show low 10's again.

I pulled the plugs after the motor blew and one of the plugs in the front rotor broke. It looks like the round piece behind the electrode flew out of there and bent the electrode on its way out. I spoke to crispeed about it and he stated that is not the cause and he thought detonation caused it and he was right.

David (rotory4life) stayed and helped me yank the motor out. Even though the plug broke in the front rotor, I was expecting just the front to be bad but a piece of one apex seal was damaged on the rear rotor. Surprisingly, the turbo was perfect, the housings were perfect and one rotor where the seal broke had some damage but good for 3mm if I cut them. All springs were perfect, side seal clearance was well within spec, quick pass of a feeler guage showed .002-.003 which surprised me. The motor was bone stock, it was weird seeing stock intake ports that small. Quick glance of the bearing etc looked good. One thing I have to add, there was ZERO carbon anywhere!!!!

At that point we cleaned all the parts to get the motor back together for summer slam but Tony had a street ported motor wrapped in plastic and decided to "lend" it to me while I get mine done the right way. I'm curious to see what a ported motor will make in HP since nothing else really is changing. So we swap oil plan etc and drop that motor in. It started up and after fixing my mistake (plugged an injector clip in wrong spot) it idled nicely and I was able to drive home an hour away.

I'll be back on the dyno this week but this time, no more methanol. I don't know why the motor blew. I was running 10.5s and I know others who ran that on C16. There was no blow by, I don't even have a catch can. The only thing I can think is the methanol being injected with E85. Enzo has repeatedly told me I don't need it but not sure if it can cause the motor to blow. My EGTs stopped working again so I don't have EGT data but air fuels on 2 widebands show low 10's and high 9s on air fuels before I was able to lean it out.

Any ideas?

Anthony

---Thanks David (rotory4ife) and my friend Kevin for helping me with everything, could not have gotten her up and running in 1 day without them. Thanks Tony from T and R Racing for the access to the dyno, lift etc and the loaner motor.
Old 06-21-09, 08:18 PM
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anthony a couple of factors could have went wrong. but usually when u see a broken apex seals you need to look into ignition timing. to much ignition timing will cause elevated combustion temperatures and detonation will be present. and not enough timing will cause your egt's to go up and a warpped apex seals is not to far along. don't go crazy looking at your air fuel mixtures being safe. but look more into your timing map. ALSO i reapeat ALSO!!! do not USE anything less then 11.5 ngk heat range for the king of horsepower levels your at.!!! any more question will be answered via pm. see you at the summer slam..
Old 06-21-09, 09:17 PM
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Glad you got it up and running again, you're the man!!!
Old 06-21-09, 09:25 PM
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Originally Posted by AnthonyNYC
I had the re-tune the because I added 2 additional 1680cc injectors for the E85. I started off on wastegate spring (17psi on my car) and made 465 with air fuels in the low 10's. I then turned on the meth injection and had to lean it out a lot (over 20%) and it made the same power. I just wanted to compare.

Now I turned up the boost to 30 psi. First pass it made just over 600 with the air fuels in the low 10's. It was a clean pass, intake temps were good, coolant temps were perfect and air fuels were perfect. 2nd pass was also perfect, made the same power. I let it cool down and wanted to run 35psi. On that pass the motor blew going into the power band. Boost did not get past 30 (same issue with this boost controller) and it was on point to making a clean pass, air fuels from the datalog show low 10's again.

I pulled the plugs after the motor blew and one of the plugs in the front rotor broke. It looks like the round piece behind the electrode flew out of there and bent the electrode on its way out. I spoke to crispeed about it and he stated that is not the cause and he thought detonation caused it and he was right.

David (rotory4life) stayed and helped me yank the motor out. Even though the plug broke in the front rotor, I was expecting just the front to be bad but a piece of one apex seal was damaged on the rear rotor. Surprisingly, the turbo was perfect, the housings were perfect and one rotor where the seal broke had some damage but good for 3mm if I cut them. All springs were perfect, side seal clearance was well within spec, quick pass of a feeler guage showed .002-.003 which surprised me. The motor was bone stock, it was weird seeing stock intake ports that small. Quick glance of the bearing etc looked good. One thing I have to add, there was ZERO carbon anywhere!!!!

At that point we cleaned all the parts to get the motor back together for summer slam but Tony had a street ported motor wrapped in plastic and decided to "lend" it to me while I get mine done the right way. I'm curious to see what a ported motor will make in HP since nothing else really is changing. So we swap oil plan etc and drop that motor in. It started up and after fixing my mistake (plugged an injector clip in wrong spot) it idled nicely and I was able to drive home an hour away.

I'll be back on the dyno this week but this time, no more methanol. I don't know why the motor blew. I was running 10.5s and I know others who ran that on C16. There was no blow by, I don't even have a catch can. The only thing I can think is the methanol being injected with E85. Enzo has repeatedly told me I don't need it but not sure if it can cause the motor to blow. My EGTs stopped working again so I don't have EGT data but air fuels on 2 widebands show low 10's and high 9s on air fuels before I was able to lean it out.

Any ideas?

Anthony

---Thanks David (rotory4ife) and my friend Kevin for helping me with everything, could not have gotten her up and running in 1 day without them. Thanks Tony from T and R Racing for the access to the dyno, lift etc and the loaner motor.

Damn that sucks, but nice that you are back in bussines!

Peter from RR was somewhat against pulling fuel out when using AI. Have you consider using straight up water instead of meth?
Old 06-21-09, 09:59 PM
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That sucks Anthony but glad you got a motor up and running again. Like Ito said, it sounds like a timing issue. Really, if your afr's were on point and egt's then timing is the only thing left unless the motor was overreved or FOB got into the engine. Oh and plus 1 on the 11.5 racing plugs.
Old 06-22-09, 04:18 PM
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Anthony, how long was the previous engine in the car for making ~600whp?

It never gets too boring with these car's thats for sure
Old 06-23-09, 07:32 PM
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pm me I got a new number, the other got "out" lol
Old 06-24-09, 12:14 AM
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Sorry to heard you blew the motor... Happy to see you got it up and running again. Good luck @ summer slam !!!! Remember you got to represent the "Yellow Rotary Community" cause ur twin brother RX7 is not ready yet (:
Old 06-24-09, 12:44 AM
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Originally Posted by KNONFS
Damn that sucks, but nice that you are back in bussines!

Peter from RR was somewhat against pulling fuel out when using AI. Have you consider using straight up water instead of meth?
I think I'll just stick to E85 for now but I understand what Peter is saying.

Originally Posted by ultimatejay
That sucks Anthony but glad you got a motor up and running again. Like Ito said, it sounds like a timing issue. Really, if your afr's were on point and egt's then timing is the only thing left unless the motor was overreved or FOB got into the engine. Oh and plus 1 on the 11.5 racing plugs.
Yeah I agree too. Timing was 14 degrees but actually lower. I forgot to make the high boost area 14 degrees so it was fluctuating between 2 cells, one cell at 14 and the other at 10. When I looked at the datalog the timing data looked squigly and then I realized why. It was hovering between 14-10 degrees. I never do that so I'm not sure if that was too retarded.

I've heard the same on the 10.5 plugs, I ordered another set of 11.5 plugs.

Originally Posted by classicauto
Anthony, how long was the previous engine in the car for making ~600whp?

It never gets too boring with these car's thats for sure
It's been in the car since early 2007 so about 2+ years now.

Originally Posted by tearbo2
pm me I got a new number, the other got "out" lol
lol, hows the beast?

Originally Posted by Judge Ito
anthony a couple of factors could have went wrong. but usually when u see a broken apex seals you need to look into ignition timing. to much ignition timing will cause elevated combustion temperatures and detonation will be present. and not enough timing will cause your egt's to go up and a warpped apex seals is not to far along. don't go crazy looking at your air fuel mixtures being safe. but look more into your timing map. ALSO i reapeat ALSO!!! do not USE anything less then 11.5 ngk heat range for the king of horsepower levels your at.!!! any more question will be answered via pm. see you at the summer slam..
Thanks Judge, I forgot the 11.5s home, next time I'll drive home for them lol. See you at Summer Slam.

On another note, when I make timing changes it makes a huge difference in air fuel ratio's. I never really read any threads about that. I went down 4 degrees and the air fuels change a whole point.

Thanks for the info.
Old 06-24-09, 12:51 AM
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Originally Posted by Travieso
Sorry to heard you blew the motor... Happy to see you got it up and running again. Good luck @ summer slam !!!! Remember you got to represent the "Yellow Rotary Community" cause ur twin brother RX7 is not ready yet (:


You better come up for Pan Ams this year!!!

Anthony
Old 06-24-09, 12:59 AM
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Has anyone ever tried the 13.5 heat range NGKs? At least thats what i think they are. They look like a surface gap plug but they are supposed to be the correct length. Just curious if it's wort it or not.
Old 06-24-09, 04:46 AM
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Originally Posted by AnthonyNYC
On another note, when I make timing changes it makes a huge difference in air fuel ratio's. I never really read any threads about that. I went down 4 degrees and the air fuels change a whole point.

Thanks for the info.
A whole point richer or leaner?
Old 06-24-09, 09:57 AM
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Sounds like an exciting day. Good luck getting everything ready.
Old 06-24-09, 11:22 AM
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My guess is the 10.5 plugs.

B
Old 06-24-09, 02:44 PM
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Talking

Originally Posted by AnthonyNYC


You better come up for Pan Ams this year!!!

Anthony
I will try , I be the one taking pictures these time... (:
Old 06-26-09, 03:45 PM
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Originally Posted by blitzboy
A whole point richer or leaner?
Leaner.


Update.....

Was on the dyno again last night, made 607HP on 30psi. Air fuels in the mid 10s. I made quite a few passes to make sure all was ok. My EGTs are still reading low but I hooked them up so I can at least compare front rotor/rear rotor. Rear rotor running very slightly leaner than the front.

After I got off the dyno, I pulled the plugs and Leading 1 was cracked with 2 small pieces missing from ceramic area. These were now 11.5's. I looked closer at Leading 2 and it had very small cracks as well but nothing flew off.

Air fuels were in the 10s. Timing was 12 deg, I was running 14 but the EGTs dropped at 12 so I left it there and it made decent power. The plugs were the same plugs from last year, I ran them a few events. I'm going with new ones.

Anthony
Old 06-26-09, 05:15 PM
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Chasing numbers

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group buy on race plugs needs to happen. I wonder how cheap we could get them if we all made a order? This $37 per plug **** is crazy!
Old 06-26-09, 05:25 PM
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Anthony, was there much of a difference in the power curves of the stock port motor vs the SP? sounds like peak power was similar.
Old 06-26-09, 11:16 PM
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Anthony,

Here is the video of that night at the dyno!!!

https://www.rx7club.com/rotary-drag-racing-167/nyce1s-com-anthonynycs-rx-7-gets-ready-summer-slam-848410/
Old 06-27-09, 01:05 AM
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Just got home from the dyno with a newer set of plugs. No more issues. Made 2 passes and left the dyno with 613HP. Air fuels in the high 10s. See you guys at Etown tomorrow.

Originally Posted by GoodfellaFD3S
Anthony, was there much of a difference in the power curves of the stock port motor vs the SP? sounds like peak power was similar.
It's hard to say, there was too much going on at the time, methanol with one vs no meth with the other, air fuels ratio's different.

Originally Posted by nyce1
Anthony,

Here is the video of that night at the dyno!!!

https://www.rx7club.com/showthread.php?t=848410
Thanks Julian, you are the man!!!
Old 06-27-09, 01:11 PM
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After I got off the dyno, I pulled the plugs and Leading 1 was cracked with 2 small pieces missing from ceramic area.
guys what would the reason be for this? just tired plugs? I've had this happen on at least one plug for the last 3 sets of NGK 10's in my car, never figured out why it was happening?


Quick Reply: Blew the motor on the dyno getting ready for Summer Slam!



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