3rd Generation Specific (1993-2002) 1993-2002 Discussion including performance modifications and Technical Support Sections.
Sponsored by:

No boost at all

Thread Tools
 
Search this Thread
 
Old 10-04-21, 02:36 PM
  #1  
Full Member
Thread Starter
 
Oppai's Avatar
 
Join Date: Apr 2020
Location: New York
Posts: 177
Received 29 Likes on 20 Posts
No boost at all

My FD recently developed an issue building boost. The car drives happily naturally aspirated and the turbos spool a little bit, but the car is only capable of boosting to atmospheric pressure and won't budge a single PSI over.

I've listened and tested for air leaks with a smoke test and soapy water on all the couplings with no luck, the car isn't making any obvious air leak noises.
I've also checked my BOV/charge relief valves for leaks and they hold pressure fine and actuate when they're supposed to.
When I let off throttle suddenly my HKS BOV will still vent but only very slightly.

Maybe there's something wrong with my wastegate/wastegate actuator?? Does anyone have ideas for other things to check?
Thanks,
Joey

Last edited by Oppai; 10-04-21 at 02:39 PM.
Old 10-04-21, 03:23 PM
  #2  
RX-7 Bad Ass

iTrader: (55)
 
DaleClark's Avatar
 
Join Date: Jan 2002
Location: Pensacola, FL
Posts: 15,399
Received 2,438 Likes on 1,509 Posts
Typically no boost means a huge boost leak. This can be as simple as a hose clamp going to the intercooler that's not tight. A visual inspection and it will look fine, but all the pressure is escaping.

Ran into that on a friend's car once - no weird noises, just non-turbo FD .

For it to be NO boost it has to be a substantial leak, not just a small vacuum hose or something.

Wastegates fail closed, so if the waste gate had some sort of problem you'd have too much boost. If the arm broke off or came off or something it would be flapping around, you'd get a metallic rattling at idle and driving around of the waste gate flapper moving.

Anyhow, I vote boost leak

Also, a smoke test may not show anything if it's a loose hose clamp or something. The smoke isn't under significant pressure, that leak is probably somewhat sealed at zero pressure.

Dale
The following 2 users liked this post by DaleClark:
Oppai (10-04-21), Retserof (10-04-21)
Old 10-04-21, 04:48 PM
  #3  
Original Owner

iTrader: (1)
 
Retserof's Avatar
 
Join Date: Mar 2005
Location: America's Dairyland
Posts: 549
Received 82 Likes on 61 Posts
As you look for those boost leaks, be sure to check the big rubber coupler that connects the top of the turbo Y pipe to the cross-over tube. They can develop a lengthwise split that opens up under boost but is nearly invisible otherwise. You may have to remove it from the car and stretch/poke at it from the inside to reveal the split.

This covers it and a lot more: FD3S:Twin Turbo Troubleshooting - Rotary Engine Wiki
The following users liked this post:
Oppai (10-04-21)
Old 10-04-21, 04:50 PM
  #4  
Full Member
Thread Starter
 
Oppai's Avatar
 
Join Date: Apr 2020
Location: New York
Posts: 177
Received 29 Likes on 20 Posts
I checked the wastegate actuator arm and the c clip had come off and left the wastegate flapping open.
I reattached the arm with a new C clip and the issue persists.. Still no boost
Haven't yet checked again to see if the new c clip also fell off since the wastegate actuator is really hot after test driving.

I've already inspected, and reinstalled all the rubber couplers besides the Y pipe coupler. Could not see any signs of a boost leak. Tried the soapy water test with the car running and also could not see any leaks out of the couplers. Where else should I check for leaks?

Last edited by Oppai; 10-04-21 at 04:53 PM.
Old 10-04-21, 04:52 PM
  #5  
Full Member
Thread Starter
 
Oppai's Avatar
 
Join Date: Apr 2020
Location: New York
Posts: 177
Received 29 Likes on 20 Posts
Originally Posted by Retserof
As you look for those boost leaks, be sure to check the big rubber coupler that connects the top of the turbo Y pipe to the cross-over tube. They can develop a lengthwise split that opens up under boost but is nearly invisible otherwise. You may have to remove it from the car and stretch/poke at it from the inside to reveal the split.

This covers it and a lot more: FD3S:Twin Turbo Troubleshooting - Rotary Engine Wiki
Thanks for the tip I checked that y pipe coupler but didn't take it completely out of the car to inspect the inside wall. Will pull it out to see tomorrow.
Old 10-04-21, 10:44 PM
  #6  
Arrogant Wankeler

 
Slides's Avatar
 
Join Date: Nov 2006
Location: Newcastle NSW Australia
Posts: 711
Received 117 Likes on 95 Posts
Secondary charge valve stuck open would do it.
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
sharingan 19
3rd Generation Specific (1993-2002)
17
09-17-10 02:10 PM
Rotors R Cool
Single Turbo RX-7's
3
01-03-09 01:34 PM
PhatManBUD
3rd Generation Specific (1993-2002)
16
01-05-06 06:43 PM
aREX4X
3rd Generation Specific (1993-2002)
8
09-06-04 08:17 AM
htharv
3rd Generation Specific (1993-2002)
8
07-21-04 04:13 PM



Quick Reply: No boost at all



All times are GMT -5. The time now is 08:08 PM.