2nd Generation Specific (1986-1992) 1986-1992 Discussion including performance modifications and technical support sections.

No boost? WTF?

Thread Tools
 
Search this Thread
 
Old Apr 13, 2003 | 09:21 AM
  #1  
Terrh's Avatar
Thread Starter
STUCK. I got SNOWNED!!!!!
Tenured Member: 20 Years
Liked
Loved
Community Favorite
iTrader: (7)
 
Joined: Mar 2002
Posts: 8,737
Likes: 20
From: Windsor, On
No boost? WTF?

'88 10AE.
Car is running PERFECT now, but I just noticed a new problem:

according to the stock boost sensor (and the butt-dyno) I'm not seeing more than 1-2PSI of boost at any time, even when I brought it from 2500RPM to redline in 3rd.

WTF is going on here?

Turbine spins freely, and I can't find any serious vacuum leaks (and wouldn't one have to be pretty damn serious to prevent almost all boost?

could my wastegate be stuck open or something?

I had plenty of boost yesterday morning, and the day before.
I ran with a (nearly) open exhauast for a bit yesterday (had to get to the parts store to get a gasket) and boost seemed to climb just fine then. Really fast, and a good amount (I let off when I hit maybe 7PSI... not much past stock.. juat wanted to hear the turbo sounds, they sould SO COOL)

Anyways, anyone have any ideas? help!
Reply
Old Apr 13, 2003 | 12:00 PM
  #2  
BlackRx7's Avatar
Daily Domestic Killer
Tenured Member 10 Years
 
Joined: Mar 2001
Posts: 2,425
Likes: 0
From: San Antonio, Tx, USA
Boost leak, even with your wastegate stuck open you'd be making 5psi atleast...check all of your intercooler hoses and what not
Reply
Old Apr 13, 2003 | 01:31 PM
  #3  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
There was a vaccume line on the intercooler that seemed to have poped off under the pressure because we dident put the clip back but thats back on and it still has the same problems. we will look harder for any other leaks.
Reply
Old Apr 13, 2003 | 07:26 PM
  #4  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
checked EVERWHERE, no leaks. WTF? Anything that could be causing this?

There's also a squeak or something, but I'm reasonably sure that it's from my air pump, not my turbo. It sounds like I ran over a little girl and she's screaming, or something.

--Terrh
Reply
Old Apr 13, 2003 | 07:38 PM
  #5  
Scott 89t2's Avatar
SOLD THE RX-7!
Tenured Member 10 Years
 
Joined: Mar 2001
Posts: 7,451
Likes: 0
From: Vancouver, BC, Canada
Re: No boost? WTF?

Originally posted by Terrh

I had plenty of boost yesterday morning, and the day before.
I ran with a (nearly) open exhauast for a bit yesterday (had to get to the parts store to get a gasket) and boost seemed to climb just fine then.
is the exhaust back on now? if so that would be my first guess if it boosted fine without it. and now won't.
Reply
Old Apr 13, 2003 | 07:49 PM
  #6  
Barwick's Avatar
SCCA Rookie
Tenured Member 20 Years
 
Joined: May 2001
Posts: 1,936
Likes: 0
From: Sterling Heights, MI
you're saying stock boost gauge? The stock gauge is CRAP.. don't trust it.
Reply
Old Apr 13, 2003 | 08:24 PM
  #7  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
it boosted VERY well with the minmal exhaust.
it boosted decently before the exhaust removal. (5-6PSI)

it boosts VERY LITTLE now. it's SLOW AS ***. Really. VERY slow. like 0-60 time of 12-13 sec, instead of 7 or 8 or whatever stock is

boost gauge (the stock one) goes to just past the zero, I know it's ***, but it is showing lack of boost, and it can do that much.

I'm reasonably sure that no giant vacuum leaks have magically appeared in the last 24 hours, but you never know... all the lines are on, and it runs fine otherwise (idle is funky, but everything else is OK)
Reply
Old Apr 13, 2003 | 08:26 PM
  #8  
Ryde _Or_Die's Avatar
...
Tenured Member 10 Years
 
Joined: Aug 2001
Posts: 7,539
Likes: 0
From: Tampa, FL
Clogged cat(s)?
Reply
Old Apr 13, 2003 | 08:30 PM
  #9  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
no, because there was boost after exhaust hookup, but there isn't now!
Reply
Old Apr 13, 2003 | 08:32 PM
  #10  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
I am going to pull the cat though.. the air line to it is gone so I might as well go all out
Reply
Old Apr 13, 2003 | 09:08 PM
  #11  
Ryde _Or_Die's Avatar
...
Tenured Member 10 Years
 
Joined: Aug 2001
Posts: 7,539
Likes: 0
From: Tampa, FL
Whose post is this? lol

Well could be a turbo going bad. My car had intermitent(sp?) boost before it went out. Any smoke ever?
Reply
Old Apr 13, 2003 | 10:26 PM
  #12  
Windsor, Ont
Tenured Member 20 Years
 
Joined: Sep 2002
Posts: 1,175
Likes: 0
From: Windsor, Ont
Originally posted by Ryde _Or_Die
Whose post is this? lol

Well could be a turbo going bad. My car had intermitent(sp?) boost before it went out. Any smoke ever?
Terrh's computer is ghetto so he comes here to use mine. but is too lazy to log out.
Reply
Old Apr 13, 2003 | 11:00 PM
  #13  
Terrh's Avatar
Thread Starter
STUCK. I got SNOWNED!!!!!
Tenured Member: 20 Years
Liked
Loved
Community Favorite
iTrader: (7)
 
Joined: Mar 2002
Posts: 8,737
Likes: 20
From: Windsor, On
yes, I'm back home. I think I'd describe my booost now as intermittent, too... I hope the turbo I bought wasn't bad! augh!

I have FULL BOOST now... 2/3 up the stock gauge, maybe a little less. car is MUCH faster, but still slow as ***... I topped out at maybe 160kph (100mph).. this sound like a clogged cat to anyone?
Reply
Old Apr 13, 2003 | 11:02 PM
  #14  
BlackRx7's Avatar
Daily Domestic Killer
Tenured Member 10 Years
 
Joined: Mar 2001
Posts: 2,425
Likes: 0
From: San Antonio, Tx, USA
one last try...is your pressure sensor hooked up?
Reply
Old Apr 13, 2003 | 11:03 PM
  #15  
Terrh's Avatar
Thread Starter
STUCK. I got SNOWNED!!!!!
Tenured Member: 20 Years
Liked
Loved
Community Favorite
iTrader: (7)
 
Joined: Mar 2002
Posts: 8,737
Likes: 20
From: Windsor, On
stupid reset form button.. dammit!

The car runs out of power above 5 grand, too.. much past that and there isn't much at all.. by 6000 its totally out of power and it seems like in 2nd or 3rd it wouldn't even get to redline.. no power up high at all... sound like clooged cat? or what? help!
Reply
Old Apr 13, 2003 | 11:38 PM
  #16  
rx7_turbo2's Avatar
Professor D.P
Tenured Member 10 Years
 
Joined: Feb 2001
Posts: 1,804
Likes: 1
From: Earth
Have you removed the twin scroll? That might be stuck shut, or the actuator or selenoid is bad.
Reply
Old Apr 14, 2003 | 10:28 AM
  #17  
Terrh's Avatar
Thread Starter
STUCK. I got SNOWNED!!!!!
Tenured Member: 20 Years
Liked
Loved
Community Favorite
iTrader: (7)
 
Joined: Mar 2002
Posts: 8,737
Likes: 20
From: Windsor, On
hmmm... I'll see if it's stuck... if I go at it with pliers it should move, right?

BUMP
Reply
Old Apr 14, 2003 | 11:58 AM
  #18  
skyypilot's Avatar
Senior Member
Tenured Member 05 Years
 
Joined: Mar 2003
Posts: 354
Likes: 0
From: Connecticut
SOunds like a stuck wastegate to me
Reply
Old Apr 14, 2003 | 12:30 PM
  #19  
Terrh's Avatar
Thread Starter
STUCK. I got SNOWNED!!!!!
Tenured Member: 20 Years
Liked
Loved
Community Favorite
iTrader: (7)
 
Joined: Mar 2002
Posts: 8,737
Likes: 20
From: Windsor, On
wastegate moves freely. is NOT stuck.
I have full boost.

car is slooooowww though. I'd estimate (butt-dyno) 90-110HP. Does feel torquey though, easy to lose the tail. but NOTHING above 5500RPM.
Reply
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Jeff20B
1st Generation Specific (1979-1985)
73
Sep 16, 2018 07:16 PM
Bauer778
3rd Generation Specific (1993-2002)
10
Nov 4, 2015 04:42 PM
t-von
3rd Generation Specific (1993-2002)
9
Sep 10, 2015 01:56 PM
High_Carb_Diet
Power FC Forum
1
Sep 5, 2015 09:07 AM




All times are GMT -5. The time now is 11:12 PM.