Single Turbo RX-7's Questions about all aspects of single turbo setups.

Annoying misfire!

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Old 06-08-11, 07:49 PM
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Exclamation Annoying misfire!

I am trying to find this "misfire" issue I am having. I have looked over and over again all wiring, coils,wires,new spark plugs ect.

35r single turbo
Stock trailing coils
Msd digital 6 + msd dual blaster coil for leading
New plugs and all 9s
Ect..

I know it maybe difficult to trouble shoot by Just listening but I'll give it a shot any way..



http://i705.photobucket.com/albums/w...r/bfa117ce.mp4
Old 06-08-11, 08:03 PM
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Idles too rich? Try 12.5-13.0 . I'm guessing its a stock port based on vacuum?

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Old 06-09-11, 02:34 AM
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Too much timing advance on idle. The miss is not that bad?
Old 06-09-11, 12:11 PM
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Did I see 207F on your external water temp gauge and 33C on your OEM sensor (Power FC)? If so one of them is wrong, and it is most likely the stock sensor. You need to get a new one. It's the one on the water pump housing. Also, if I'm right you are running an FC thermoswitch which is turning on your #1 fan relay at 97C/207F. Your ECU is not engaging the #2 and #4 fan relays because the water temps are reading too low.

Also, with a bad water temp reading you will be stuck in warm up enrichment and depending on your setup it will affect your ignition timing as well. Both can contribute to misfire at idle.
Old 06-09-11, 01:14 PM
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Yeah I have the FC thermo switch and the water temp sensor was installed new by me like two years ago... I have the digital temp gauge hooked up from the rear housing coolant nipple to the top coolant nipple on top of the water pump housing. Is it possible I have the water temp green connector the the fuel rail temp connector swaped?
Old 06-10-11, 08:06 AM
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(Arghx) good eye. Yeah I had the fuel rail sensor and the temp sensor swaped... I swaped them to their right location and right away the a/fr came up in the mid 12s at idle... I am going to take it for a spin today and report back, thanks guys...
Old 06-10-11, 09:34 AM
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Good thing u have the fc thermoswitch. Otherwise your fans wouldn't come on until very late.

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Old 06-10-11, 11:24 AM
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It's so easy to mix up them two plugs, Mazda should have made them a diffrent color or connector ..
Old 06-10-11, 12:16 PM
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Glad to see you finally using those electronics
Old 06-10-11, 12:33 PM
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Originally Posted by MOBEONER
It's so easy to mix up them two plugs, Mazda should have made them a diffrent color or connector ..
Well to be honest I'm not sure how you mixed them up. they're kinda positioned where they need to be lol. But **** happens I guess.

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Old 06-10-11, 01:38 PM
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Originally Posted by thewird
Well to be honest I'm not sure how you mixed them up. they're kinda positioned where they need to be lol. But **** happens I guess.

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Haha yeah!! I did a single turbo harness Conversion and I must have mixed them both and some how they Both looked the same length,but yeah I am glad it was a simple fix. . I was starting to think the motor had some sort of mechanical issue..
Old 06-10-11, 01:52 PM
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Originally Posted by beefhole
Glad to see you finally using those electronics

Haha that's funny, i was going to call you to ask you about this as well.
Old 06-10-11, 02:49 PM
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forgot about the whole swapping thing. yes that is a pretty common mistake
Old 06-11-11, 01:08 AM
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So i took her for a ride and shes running much better now but shes leaning out on me. At idle shes about 12.3 12.5 when i start driving and accelerate lightly she goes from 12 A/Frs to 15 and 16 and she bucks..... I checked fuel gauge 38 psi at vaccum, replaced fuel filter, pump is working ...
Old 06-11-11, 08:52 AM
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Always run rich, and take away fuel where you don't need it.

16 is safe under cruising/vacuum, but all engines are different.

Mine is also unhappy above 16. Some can do 17-18, but everyone is different.
Old 06-11-11, 03:24 PM
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When my gauge hits upper 15 to 16 it bucks...
Old 06-11-11, 05:01 PM
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Is this new or has it always done that? This is under throttle tip-in or during steady throttle position?
Old 06-11-11, 05:33 PM
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Originally Posted by arghx
Is this new or has it always done that? This is under throttle tip-in or during steady throttle position?
It just started doing that. I am running the same set up as last year exept this year i installed the 35r single turbo kit. I am runing same fuel set up 550/1300 with stock map and changed the 850 to 1300 on power fc/datalogit . I downloaded one of chuck.W map and loaded it to see if it was a tuning issue and it still does the same thing... I checked fuel filter,fuel pump,FPR and all injector connectors, The FPR vaccum hose works.. I dont know whats going on..

I am just begining to understand The PFC and how it works and tuning but i have not tried to mess around with anything in the PFC.

This is under throttle tip-in or during steady throttle position?
I would have to say both... even when parked, i rev the car and keep (lets say) a stedy 4,000RPM rev it leans out in and out...I will take video of what it does and post it...
Old 06-11-11, 05:46 PM
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Datalogs would help, preferably ones where you have a wideband input. You loaded a map that hasn't been specifically optimized for your car so there is no guarantee that it isn't still a tuning issue. A single turbo conversion is a big enough change that it can throw off the tune even though you didn't change injectors.
Old 06-11-11, 06:03 PM
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Originally Posted by arghx
Datalogs would help, preferably ones where you have a wideband input. You loaded a map that hasn't been specifically optimized for your car so there is no guarantee that it isn't still a tuning issue. A single turbo conversion is a big enough change that it can throw off the tune even though you didn't change injectors.
Thanks,i will try and datalog and report back. I am still very fresh at it so i will read up on how to datalog correctly. By the way i dont have my wideband connected to the datalogit. is that a problem?
Old 06-11-11, 07:17 PM
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without having it hooked up you will greatly limit the usefulness of the logs
Old 06-12-11, 05:28 PM
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This was me reving the motor while in park..If I'm not mistaking the secondary's are the problem.
I checked connectors and everything is connected.

Old 06-12-11, 05:42 PM
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I'm no expert, but I'm thinking the split should be more consistent under vacuum. It starts at 12, but when you touch the throttle, it drops to 3

Tighter split = leaner right?

Also the secondary injectors shouldn't be coming on under vacuum, unless the computer is supposed to fire all 4 for tip in?

I do not know the PFC like my old haltech though

Any experts feel free to chime in!
Old 06-12-11, 06:00 PM
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Nothing looks wrong in the log. Have you tried adding fuel in that area?

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Old 06-12-11, 06:10 PM
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I have not touched a thing. All I did was install a diffrent map to see what would happened and still the wideband goes lean and bucks. I will post a video of what it does..

Here is video.
http://i705.photobucket.com/albums/w...r/48e269f2.mp4


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