Haltech Forum Area is for discussing Haltechs

Haltech Blew the motor.........

Thread Tools
 
Search this Thread
 
Old 03-06-08, 12:44 PM
  #1  
Senior Member

Thread Starter
iTrader: (3)
 
SHPNOUT's Avatar
 
Join Date: May 2001
Location: BENICIA, CA
Posts: 482
Received 7 Likes on 7 Posts
Blew the motor.........

Hey Gents,
First post to this section.

A bit of back ground. 13bTT, Pettit hi flow turbo's non sequential.
This is from Pettits old GT2 racecar.

Car has run reliably with Haltech E6S forever. Rock solid tuned for 15lbs max, I was running 13.5 to 14. Gas 110 octain. (overkill)

Cold morning, car would not start with cold plugs in (not surprised). Switched to warm plugs 9's to get started. While doing so I broke the lead to the top crank angle sensor top pin (of the two) lead. I quickly repaired so I cold make my session. Car ran fine. Half way thru the session the front apex seals blow.

Question - could a poor conection in that location of the crank angle sensor cause the motor to go lean and pop? Could it be a bad coil pack? All plugs had spark, Front lower seemed weeker then others after the fact.

This car has had NO issues prior to this day. Runs/ Ran llike a rolex watch. Never overboosts, always runs cool. Perhaps to cool.

I am a long time rx owner but this is my first dive in to motor building and haltech .

Thanks
Niles
Old 03-06-08, 01:16 PM
  #2  
slo
registered user

iTrader: (1)
 
slo's Avatar
 
Join Date: Jan 2006
Location: San Diego
Posts: 2,469
Likes: 0
Received 0 Likes on 0 Posts
Not necessarily lean, a poor connection or even mis routing the wires, can cause noise in the pickup that will make the haltech all fucked, often intermittently.

I mean misfiring, radical advanced or retarded ignition, missing injection events, putting in extra injection events.

One or more of these can be results of trigger issues that can and will blow an engine.




Originally Posted by SHPNOUT
Question - could a poor conection in that location of the crank angle sensor cause the motor to go lean and pop? Could it be a bad coil pack? All plugs had spark, Front lower seemed weeker then others after the fact.
Old 03-06-08, 01:24 PM
  #3  
eccentric shafter

 
rotary8's Avatar
 
Join Date: Oct 2007
Location: EARTH
Posts: 143
Likes: 0
Received 0 Likes on 0 Posts
Blew the motor.........

first of all 13.5 to 14.0 air to fuel ratio is no good for a turbocharged rotary worst on a cold day you should be at 11.5 air to fuel ratio. It sounds to me like you created your own problems which blew the engine.
Old 03-06-08, 01:28 PM
  #4  
www.lms-efi.com

iTrader: (27)
 
C. Ludwig's Avatar
 
Join Date: Mar 2001
Location: Floyds Knobs. IN
Posts: 5,236
Received 129 Likes on 85 Posts
Originally Posted by rotary8
first of all 13.5 to 14.0 air to fuel ratio is no good for a turbocharged rotary worst on a cold day you should be at 11.5 air to fuel ratio. It sounds to me like you created your own problems which blew the engine.

He was referring to how much boost he was running.

Agree with Slo. If your quick and dirty fix on the trigger was too dirty it could of caused all kinds of havoc.
Old 03-06-08, 01:36 PM
  #5  
Senior Member

Thread Starter
iTrader: (3)
 
SHPNOUT's Avatar
 
Join Date: May 2001
Location: BENICIA, CA
Posts: 482
Received 7 Likes on 7 Posts
Yep, those were boost #'s.

Thanks for the info, I figured as much......

That said, .....What is a good way to go with this connection........Pictures would be great.

Thanks
Niles
Old 03-06-08, 02:10 PM
  #6  
Crash Auto?Fix Auto.

iTrader: (3)
 
classicauto's Avatar
 
Join Date: May 2003
Location: Hagersville Ontario
Posts: 7,831
Likes: 0
Received 2 Likes on 2 Posts
I think a better question would be how was the lead broken/repaired?

If its boke on the sensor side only, and the connector on the harness is alright, I'd just find another sensor/pickup in the classifeds. But if the harness portion is damaged, I'd be hunting for some new sheilded cable....
Old 03-06-08, 02:27 PM
  #7  
Senior Member

Thread Starter
iTrader: (3)
 
SHPNOUT's Avatar
 
Join Date: May 2001
Location: BENICIA, CA
Posts: 482
Received 7 Likes on 7 Posts
The female fitting on the end of the lead broke off. I cut the wire, stripped it and reused the old lead. A $4k wiring job.

New cable?
Old 03-06-08, 02:31 PM
  #8  
slo
registered user

iTrader: (1)
 
slo's Avatar
 
Join Date: Jan 2006
Location: San Diego
Posts: 2,469
Likes: 0
Received 0 Likes on 0 Posts
Originally Posted by SHPNOUT
The female fitting on the end of the lead broke off. I cut the wire, stripped it and reused the old lead. A $4k wiring job.

New cable?
If it broke off then the wire was probably in real bad shape...
Old 03-06-08, 04:16 PM
  #9  
Senior Member

Thread Starter
iTrader: (3)
 
SHPNOUT's Avatar
 
Join Date: May 2001
Location: BENICIA, CA
Posts: 482
Received 7 Likes on 7 Posts
slo.......thanks for your help.
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Logan Reinisch
General Rotary Tech Support
44
09-17-18 12:20 PM
7upra
New Member RX-7 Technical
5
03-25-18 11:32 AM
R|©haźd
New Member RX-7 Technical
1
09-24-15 11:39 AM



Quick Reply: Haltech Blew the motor.........



All times are GMT -5. The time now is 03:17 PM.