3rd Generation Specific (1993-2002) 1993-2002 Discussion including performance modifications and Technical Support Sections.
Sponsored by:

pleasant surprise, but how did it happen

Thread Tools
 
Search this Thread
 
Old Oct 27, 2002 | 03:42 PM
  #1  
bploz RX7's Avatar
Thread Starter
Full Member
Tenured Member 10 Years
 
Joined: Apr 2001
Posts: 242
Likes: 0
From: marietta, ga (soon 2B san diego)
pleasant surprise, but how did it happen

This is the first time I have had a good surprise from my FD!! I have had 6-7 lbs. of boost on my primary w/ no boost on the secondary for a good 6 months now. I just assumed it was vacuum line related and w/ 77k on the engine (and it being just a weekend car) I was in no hurry to do the vacuum job until I got a rebuild. I thought the rebuild was just around the corner since it took a little longer to crank over, extra smoke at start-up, low vac. readings at idle, etc. Well the past 2 weeks I have had to use it as my daily driver and thought nothing of it until today. I started it up and the exhaust note was deep and throaty and was popping/backfiring like it used to when driving it cold. So after it gets to normal operating temp I give it gas and primary boost jumps to 12lbs. and holds perfectly. Then to my amazement my secondary comes on and holds 10 lbs to redline!! I almost wet my pants because I forgot what kind of power these bad boys have. Can anyone give a little insight as to what happened?? My mods are the typical exhaust, intake, and upgraded ECU (all Pettit products). Could the hi-flo cat have been clogged??

Thanks for your input,
Brett
Reply
Old Oct 27, 2002 | 05:24 PM
  #2  
sanfordman's Avatar
Full Member
Tenured Member 20 Years
 
Joined: Apr 2002
Posts: 176
Likes: 0
From: raleigh, nc
sounds like a secondary turbo vac line prob, open up your hood and look at the black box in front of your manifold and check to see if you have a loose vac line going into the black box or underneath it (only 2 bolts). maybe you had a loose actuater and it got reattched somehow.........??but I would check in there and see if anything is amiss, do us all a favor now that you have full boost and embaress some of those yuppies in their corvettes!!
Reply
Old Oct 27, 2002 | 06:06 PM
  #3  
spooledUP7's Avatar
There and back again
Tenured Member 15 Years
 
Joined: Feb 2001
Posts: 967
Likes: 0
From: Camarillo, Ca
When I was sequential, I pulled chunks of hair out trying to figure out why they would work some times, but not others. There were times when all did between non-working, and properly working turbos was remove a single line an put it back on. It's a mystery to me how it would have helped, but it is possible that simply driving the car was enough catylist for something to happen.

If I were to take a guess, I would say that something like dirt and oil finally blew past a check valve, or solenoid passage. It could have been a bad harness connection, or piece of carbon builup flaking off one of the control doors.

I'm glad you got the chance to feel the power again. I just hope it lasts more than the next start up.
Reply
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
binz
3rd Generation Specific (1993-2002)
7
Oct 2, 2015 03:52 PM
musker
New Member RX-7 Technical
1
Oct 1, 2015 05:58 PM
izzolaw
Introduce yourself
1
Sep 28, 2015 06:03 AM




All times are GMT -5. The time now is 11:22 AM.