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Boost problem when shifting above 4k

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Old Apr 19, 2005 | 12:25 AM
  #26  
Xeros's Avatar
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I'm sorry wha?
Tenured Member 10 Years
 
Joined: Aug 2003
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From: Wisconsin
Others should post thier solutions to this problem as well if Diffrent. That way this thread can be stickied or archived or whatever for future users.
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Old Apr 19, 2005 | 03:33 PM
  #27  
WaLieN's Avatar
Call me gramps!
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From: Detroit, MI
Originally Posted by Xeros
problem solved. Well my problem has been solved let this be a sticky....Here is what I did. I took off my UIM....I noticed that my turbo control solenoid (the one on the LIM) vacuums hoses were being sqeezed off becasue they had a 90 degree bend in them. going from the solenoid that sits on the LIM to the rats nest. So I took em off and replaced them with somelonger ones that bent in such with out squeeziing the air off. I then proceeded to make my boost controller nipples a bit larger becasue I wasn't able to let enough air pass through last time around to get the primary turbo down to 10 psi. After a couple of test drives I adjusted my valves to a pervfect 10 -9-10 pattern. When I shift the PSI now keeps at 10 psi with the second turbo.
Hehe, I knew it was either a problem with the lines going to the TCA/TCS! Anyways, I am glad you solved it. Doesn't a 10-8-10 boost pattern feel nice?
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Old Apr 19, 2005 | 05:39 PM
  #28  
Xeros's Avatar
Thread Starter
I'm sorry wha?
Tenured Member 10 Years
 
Joined: Aug 2003
Posts: 1,098
Likes: 1
From: Wisconsin
yes and no.....hahah...I really shouldn't be going over 4000 seeing as how I only have like 600 miles on my new engine....but it was somehting that was bothering me quite a lot and i wanted to taker care of it right away.
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Old Apr 25, 2005 | 04:14 PM
  #29  
gravytrain15's Avatar
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Tenured Member 05 Years
 
Joined: Apr 2005
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From: Plainfield, Vermont
newbie here......i've had the same problem with my fd. boost falls off over 4k, crank angle sensor was to blame....serious problem that did not throw the check engine light, had to jump the diagnostic ground an ten pins.that gave me the code. besides that i have been in the market foran apexi power FC. is the 95-98 model ecu the same, my car is a 93 and i could get a good deal off a friend if they are compattable.

ps, hes a wuss so he wont let me just plug it in and see, hes afraind it may mess up the brain.
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