Fuel cut on my Rx with rtek system??
#1
Fuel cut on my Rx with rtek system??
hey guys, i did a quick search didnt really find any thing, so heres the story:
been noticing on a very slight throttle, the ex. pops, which i think its always done
but now, when im completly of the throttle, in gear, decel., the ex. pops in
and around 2k. but didnt really think anything of it.
lastnight, right before going out to race, on a slight throttle(keeping speed)
the car would buck a bit, but not bad.
i raced a mustang on 15psi, and pulled him, but because of other races going on
behind us, i didnt feel like it was a fair race to him, so asked if he wanted to go
again.
went out and in 1st gear (20mph roll) race was bucking kinda bad. so asked
if we could roll a 40 (2nd gear launch) started the race and pulled hard for a sec.
the NOSE DIVED!!! couldnt figure out the problem, at this point on decel. ex. is
popping a lot.
we head out and i notice at idle its SUPER LEAN like my AFR gauge isnt even
showing a number, dont know how it idled. cruising at 60 the afrs, sometimes
dipped lean, but would come up.
so i decided to do another test, and get into boost. as soon as i got to 5-6psi,
its like it was fuel cutting, afrs would go super lean again.
any ideas??
any help would be great.
thanks
been noticing on a very slight throttle, the ex. pops, which i think its always done
but now, when im completly of the throttle, in gear, decel., the ex. pops in
and around 2k. but didnt really think anything of it.
lastnight, right before going out to race, on a slight throttle(keeping speed)
the car would buck a bit, but not bad.
i raced a mustang on 15psi, and pulled him, but because of other races going on
behind us, i didnt feel like it was a fair race to him, so asked if he wanted to go
again.
went out and in 1st gear (20mph roll) race was bucking kinda bad. so asked
if we could roll a 40 (2nd gear launch) started the race and pulled hard for a sec.
the NOSE DIVED!!! couldnt figure out the problem, at this point on decel. ex. is
popping a lot.
we head out and i notice at idle its SUPER LEAN like my AFR gauge isnt even
showing a number, dont know how it idled. cruising at 60 the afrs, sometimes
dipped lean, but would come up.
so i decided to do another test, and get into boost. as soon as i got to 5-6psi,
its like it was fuel cutting, afrs would go super lean again.
any ideas??
any help would be great.
thanks
#4
yes its an s4, engine is an 88 to be exact
mods:
FMIC
GReddy throttle tube
moded TB
2.5" IC piping
emision delete
airpump delete
60-1 to4e w/.82 a/r
3" ex. (open DP right now)
tubular manifold
38mm WG
Apexi AVCR
Rtek 2.1
No Porting
i may be leaving something out, not 100% sure but i think thats it
mods:
FMIC
GReddy throttle tube
moded TB
2.5" IC piping
emision delete
airpump delete
60-1 to4e w/.82 a/r
3" ex. (open DP right now)
tubular manifold
38mm WG
Apexi AVCR
Rtek 2.1
No Porting
i may be leaving something out, not 100% sure but i think thats it
#6
Rotary Revolutionary
iTrader: (16)
+1 this sounds like a fuel problem.
(problem #1 ....I see no injectors or pump on that mod list )
Have a look in the tank, the sock could be clogged
When was the last time you changed your fuel filter?
Verifying fuel pump voltage is a good idea, and while your at it, check the actual connections at the pump to make sure nothing has giggled, or corroded its way loose.
(problem #1 ....I see no injectors or pump on that mod list )
Have a look in the tank, the sock could be clogged
When was the last time you changed your fuel filter?
Verifying fuel pump voltage is a good idea, and while your at it, check the actual connections at the pump to make sure nothing has giggled, or corroded its way loose.
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#8
ran a diagnostic on my Rtek:
Errors:
Tps sensor (narrow)
so ill swap that out and see how it goes.
do tps go out just suddenly like that?
when i was running the log the tps was working for a min.
then went to 100% all the time
ill post results after replacement
Thanks for the help!
Errors:
Tps sensor (narrow)
so ill swap that out and see how it goes.
do tps go out just suddenly like that?
when i was running the log the tps was working for a min.
then went to 100% all the time
ill post results after replacement
Thanks for the help!
#9
well the tps helped, but its still not running good
still cutting out from 2-5psi.
almost sounds like what it would be if i slipped an IC coupler, but ive checked them all and
their good and tight
ive got 3 logs just cant tell what any of it means lol.
if i can figure out how to get it on here ill post it.
still cutting out from 2-5psi.
almost sounds like what it would be if i slipped an IC coupler, but ive checked them all and
their good and tight
ive got 3 logs just cant tell what any of it means lol.
if i can figure out how to get it on here ill post it.
#11
Rotary Revolutionary
iTrader: (16)
This doesn't sound electronic... unless its related to the boost controller or the fuel pump isn't seeing proper voltage. If its running lean (and there have been no changes to the maps/timing) either A) Its not getting enough fuel ....or B) Air is sneaking in somewhere.
Pressure test both the intake track and the fuel system, and I'm pretty sure it'll get you headed down the path to recovery.
Pressure test both the intake track and the fuel system, and I'm pretty sure it'll get you headed down the path to recovery.
#13
yaa... so i pretty well just hate Rtek... old *** technology..
it wont hotsync to my computer, wont even bluetooth hotsync
the only thing done on the logger, was to richen up, it had been showing rich up untill this..
what i saw on the logger was that it would just barely get into boost. 2-5psi, REFUSED to
go higher then that
heres values i logged right at ''fuel cut''
rpm: 4040
airflow: 15.1 lbs/min
map: 2.2 psi
tps: 94% (swapped out the one that was broke for on that read max on 94%, not great
it works for now)
intake air temp: (88.2*F)
timing L: +13.3 degrees
timing T: -1.8 degrees
O2(still doesnt work???) 0.03volts
Right at this point in the logger, the afr gauge face plants lean, like doenst even give a numerical value
ive dont this several times, soo if it would help to post more of these values right at F-UP,
i can
it wont hotsync to my computer, wont even bluetooth hotsync
the only thing done on the logger, was to richen up, it had been showing rich up untill this..
what i saw on the logger was that it would just barely get into boost. 2-5psi, REFUSED to
go higher then that
heres values i logged right at ''fuel cut''
rpm: 4040
airflow: 15.1 lbs/min
map: 2.2 psi
tps: 94% (swapped out the one that was broke for on that read max on 94%, not great
it works for now)
intake air temp: (88.2*F)
timing L: +13.3 degrees
timing T: -1.8 degrees
O2(still doesnt work???) 0.03volts
Right at this point in the logger, the afr gauge face plants lean, like doenst even give a numerical value
ive dont this several times, soo if it would help to post more of these values right at F-UP,
i can
#15
ya myabe, what sucks is the ONLY place i could find one was at the pawnshop..
and i got the best there, the T|X. def not happy with the hardware, as far as tuning, love it.
just wish they'd atleast do a laptop program........aaahhh sorry was dreaming of the simplicity. lol
not sure guess i need to log that as well, not sure of that either actually.. they are set to come on at about 3300rpm
ill do somemore logs, with these values u said, and someothers.
and i got the best there, the T|X. def not happy with the hardware, as far as tuning, love it.
just wish they'd atleast do a laptop program........aaahhh sorry was dreaming of the simplicity. lol
not sure guess i need to log that as well, not sure of that either actually.. they are set to come on at about 3300rpm
ill do somemore logs, with these values u said, and someothers.
#16
would boost sensor caused this?
i got tps back into adjustment.
the test i did was i left the boost sensor harness unpluged, and it runs the same as it has been. which leads me to beleave its the problem.
it makes sense to be the boost controller, there arent any air leaks, as far as i can tell.
its getting fuel while driving, highway or in town, but when i get into boost fuel cuts.
and the timing doesnt seem to be off.
any input?
thanks!
o oo oooo and a dumb question, is there a difference between turbo and non-turbo sensors?
i got tps back into adjustment.
the test i did was i left the boost sensor harness unpluged, and it runs the same as it has been. which leads me to beleave its the problem.
it makes sense to be the boost controller, there arent any air leaks, as far as i can tell.
its getting fuel while driving, highway or in town, but when i get into boost fuel cuts.
and the timing doesnt seem to be off.
any input?
thanks!
o oo oooo and a dumb question, is there a difference between turbo and non-turbo sensors?
#19
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Join Date: Mar 2006
Location: Pottsville PA
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i had a similar problem...turned out my fuel pump strainer was blocked...take the 10 minutes and pull your pump...spray the sediment off with carb cleaner...hope this helps you
#21
WWWWOOOOOOOOOOOOOOOO!!!!!!!!!!
i checked the filter sock, it was a little dirty, so i said screw it and swapped the pump and sock
all together.
but i do know what the problem is!!! i think...
did a log, and the 2ndry flag stays off!!!
would that feel like fuel cut??
why are the 2nds not coming on?
what do i need to do to fix this??
is this an ecu issue?
Any help would be great
i checked the filter sock, it was a little dirty, so i said screw it and swapped the pump and sock
all together.
but i do know what the problem is!!! i think...
did a log, and the 2ndry flag stays off!!!
would that feel like fuel cut??
why are the 2nds not coming on?
what do i need to do to fix this??
is this an ecu issue?
Any help would be great