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the gauges pointed toward you is a thing! mine are in a similar spot, but they just face i guess the spare tire. the fan comes on when its supposed to, at like 100c or something, but with the parallax view, it looks like 110c! which is scary. at 90 the needle is straight up, so it looks right, its kind of odd
Since mine are digital parallax isn't a problem, but I was trying to minimize taking my eyes off the road. Averting my eyes briefly isn't an issue but needing to turn my head or crane my neck is. A-pillar or warning light locations would be better, but like I said, I prefer OEM-like.
I actually guessed on the angle, 15 degrees in two axes was the most I could fit, and it landed in the perfect place
Nice job on the panel. I wanted to do the same thing for the multi, O2 and alpine controller but now it's just the alpine since I'm not using the other two. Maybe a giant printed cubby hole now?
I think printing a new mirror control panel with a phone tray and provisions for a charging coil would be a cool idea also.
I can share the blank plate with you (I have a version with the mounting provisions but without the cutout for the gauges), it shouldn't be hard to add a cubby.
The only hard part is the angle of the roof of the cubby isn't orthogonal to the front plate, it has a slope to it. And I'm an amateur, so I'm sure there is a function for that in Blender but I'd have to take the measurements of the angles and do the trigonometry on paper to figure it out for an exact fit.
I was able to find some more time to work on my Rx7. The work was done piece-meal over the past few weeks when I had time between exams, so apologies if this update is a bit scattered.
There were two issues (broadly speaking) that I wanted to deal with. First was the steering issue, since that is a safety concern. Basically it was heavy in a few spots at idle, but then at speed it was a bit reluctant to return to center without correction and had a very slight loose spot in the middle. I knew that the adjustment on the steering rack for the yoke support was a bit fiddly, but couldn’t find anything wrong with it. Then I read something interesting in the Series 4 training manual about how the rack yoke support had been “changed to a ball-bearing type”. I didn’t remember any ball bearing on mine. So I pulled it out:
The top is the adjustment bolt and lock nut. The little spring fits in the cup on the left, and the cup rides against the steering rack. This way you can adjust the tension using the bolt and then lock it with the ring. I turned over the cup piece to look at the rack side, and I didn’t see a ball-bearing. But then I cleaned away the grease…
Aha! So that was why it went from too loose to too tight with no in-between. The ball-bearing must have gotten lost when I rebuilt the rack. The local Mazda dealership doesn’t list a part number for this piece (the ball-bearing or the yoke itself). He was kind enough to make some calls for me and find that the part is completely NLA. So it’s time for a DIY solution.
I measured and found the ball-bearing to be about 5mm in size. I found you can order ball bearings on eBay for like $2 a bag, so I ordered 5mm and the size just above and just below:
From China to my doorstep in less than two weeks… What a time to be alive; this sort of thing would have been a real hassle just a few years ago.
5mm fits and is the closest, although if I could find 5.1mm or 5.2mm it might be better. 5.5mm is the next size up that I have, and is too big. I have plenty of leftovers, so if anyone needs ball-bearings, let me know and they’re yours…
It’s a pretty good fit. Certainly good enough to use. I added some extra grease to the rack and pinion through the yoke adjustment opening:
I just kept adding grease and carefully packing it down underneath the rack, and it kept taking more. A bit unusual since I greased it thoroughly when I reassembled the rack, but oh well. I may take it back out soon and see if I can get more grease in there. Anyways, after putting yoke adjustment back together and tightening to the factory spec, it’s much better!
Still not quite perfect. I found that the idle dips when turning the wheel if accessories are on at the same time, so the ECUs idle system is not quite handling things like it should. This is causing a bit of heaviness at idle still, under certain conditions, but no more tough spots. And the steering at speed no longer has that loose spot in the center, but every so often it’s still a bit reluctant to return to me on it’s own. Going to have to play with the adjustment a bit further I think to sort that out. Either way, it’s certainly good enough to drive and enjoy
Then I took care of a few small maintenance items, before moving to the next issue. An oil change is a good idea, since it’s been about a year and this is the first change for this engine. We have little oil change pit off our driveway that makes the job easy:
I just use conventional. I have no qualms running synthetic, but since rotary engines dilute oil with fuel so quickly you don’t really get to make use of the extended oil change interval, so IMO it’s a waste of money. On a turbo engine with higher oil temps, I would run it though. I like the Fram Gold-can filter, since testing I saw a few years ago put it at the top in terms of filtration.
Then my air filter. This was pretty clean when I started driving the car last year, but I’m glad I inspected it:
Over the winter the mouse decided to stow some leaves in here. Curiously, he also seems to have a fondness for push-pin fasteners…
Yikes! New filter to the rescue:
This one includes a nice mesh that will hopefully prevent rodent damage in the future. Won’t stop the little guy from living in there, but at least he can’t tear holes in it again. The colour is quite festive as well.
I also replaced the fuel filter. Lost the pictures, but you all know what a fuel filter looks like.
Then some spark plugs. Previous set was re-used from my previous engine, and weren’t really all that bad. But I wanted to address an issue I’ll talk about later, so it was a good idea to replace them anyways:
Got some nice new NGKs.
Leading in center, trailing on right. The trailings weren’t that bad, but the leadings are getting a bit worn.
And while all of the above was a good idea, none of it addressed the second issue I’m having. I am getting these small hesitations under load, at certain areas in the rev range. 3800rpm is a common issue because of the secondary injectors, but I’m getting it other places as well. My grounds are good, my plugs are good, plug wires, etc. The two things I thought could be suspect are the MAF sensor and the fuel pump. Now I’ve replaced both, but they could still be potential causes of the issue. As far as testing the MAF, I pulled it out when I had the airbox out for the filter change. Then I powered it on the bench and measured the output:
Borrowed the cable from an old Nortel linesman’s telephone I had around to convert the bench supply to alligator clips. Then clipped them to the ground and VCC of the MAF. I also removed the silicone-sealed cap on top of the MAF to look inside, but nothing seems unusual. Then to measure the sweep of the sensor, I needed an analog voltmeter to see if the reading was smooth or if it was jumping around. Luckily I’m well equipped in that department:
It moves smoothly from 4.5V at full closed to about .5V at full open. Which tells me the MAF is probably fine. So I reinstalled the cap with fresh silicone, and put it back in the car.
As for the fuel pump, I replaced it (including fresh wiring) a couple months after I got the car. This would have been 4-5 years ago now. Turns out when I went to inspect that 18 year old me and current me have different ideas of what constitutes acceptable wiring:
It’s more painful when you can’t blame the previous owner for the terrible work. This one’s on me. Luckily I had this connector around already, so I was able to refresh everything without waiting on parts:
I don’t have the crimping tool for these, so I crimped them manually and added some solder as insurance. Then popped them into a new connector:
Better. The harness side was in fine shape, but I replaced the connector anyways since I had the set. I also rewired the fuel pump awhile back, with a fresh 10 gauge power wire straight from the fuse panel and a relay on the original wiring. The harness side being good and the connector from the pump being fixed, it was time to look at the fuel pump flange:
Surface rust aside, I don’t trust that ground. The original ground looks like it broke off and the fastener was seized, and then I decided to ground it using one of the mounting bolts. Not the worst thing in principle. But just looking at this I can guarantee there is voltage drop across that ground.
So I took the assembly out of the tank and sprayed all the fuel out with carb cleaner. A torch made quick (albeit nerve-wracking) work of the stock ground tab and freed the stock fastener, and a wire wheel cleaned the rust off.
Then I cleaned a flat spot to add a second ground point:
Welding was a bit nerve-wracking too, since this was bathed in fuel just a few minutes prior. No drama though. I welded the first M6 nut on, then the bolt broke off inside it. I’m assuming it warped from the heat. So then I welded the second nut on top of the first nut, and this one threaded in fine. Then I split the ground wire and crimped new ring terminals, so now it uses the stock ground point as well as the new one. This gives me some redundancy. Some dielectric grease helps keep them protected. I measured zero ohms between the negative terminal on the pump and the spade in the connector, so we’re good to go.
I also re-flowed the solder joints on the other connections on the pump and added fresh marine heat-shrink tubing:
This is like the regular stuff, except it includes a water sealing adhesive on the inside of the tubing. Great stuff and not much more expensive than regular. The fresh foam is there just because the original stuff perished from age. Forgive the lighting, most of this was done past 10 at night.
And well, there is no apparent difference to the hesitations. At least I know the pump is not the culprit.
As far as what could be causing the hesitations, I’m out of ideas. I’ve checked, rebuilt, or replaced literally every part of this car. I could look around for another MAF, but since this one checks out I highly doubt that’s the culprit. Basically it would just be throwing parts at the problem. Everything is adjusted as per the FSM, all the grounds are good, all the maintenance items are good. I’m kind of out of options. I’m just going to live with it for now while I think about possible causes, since it isn’t a safety issue. But it certainly is annoying.
Lastly, I washed the car and took some pictures:
And that’s it for now. Other than adjusting the steering a bit and the hesitations, everything on the car kind of just works as it should. So for now I’ll just drive it and keep thinking on the issue.
Just like that, my hesitations are gone. I can still feel the secondary changeover at 3800rpm, but it's no longer a violent bucking.
What was the fix? I removed all ECU / sensor grounds I added. It makes no sense, but maybe the ECU cares that all the sensors ground in the same place and have identical voltage drop. I had figured that everything grounding to the body was better. But the only ground left for the ECU + all the sensors is the one on top of the engine block, and now the engine is very happy.
I've learned not to question these things anymore. The Rx7 giveth and the Rx7 taketh away, so I'm just going to enjoy driving it while it giveth.
Awhile back I made a sort of custom short shifter. I took the bottom spherical part that fits in the shift block from a stock Rx7 S4 shifter, welded it to an eBay Miata short shifter since the Miata uses a smaller diameter ball, then cut off the threaded part up top and welded on an M10x1.25x50 bolt to use my preferred shift ****. It worked fine, but the extra long threaded section (my shift **** is weirdly tall) made it so it was about stock height. The throw was still shorter due to the fulcrum being farther from the shift block, but the shifter just sat a bit too tall.
Here's a picture from a previous update not long ago for reference:
You can see the height issue. So I took off the boot and examined to see how much length I could take out. Pardon the photo quality, this was done at 10pm my time and the only illumination is the map light:
The shifter is two pieces, making removal significantly quicker. If I wanted to get extreme, I could cut it as low as the threaded section. But then it's always easier to take out material than to add, so I decided to start where the wide section begins to taper.
Two cuts and a weld later:
As you can see, I come from the "pile it on and pray" school of MIG welding.
Then a lick of paint to prevent it rusting:
And finally, possibly the worst photo I've ever taken:
Now it finally feels right, although I'll definitely need to do something about the shift boot. Maybe take out 1-1.5" of material. I'm going to drive it a few times and make sure I'm okay with this height before I commit, since my shift boot is in nice shape and I'd hate to ruin it.
Have a set waiting for mine, ordered a set for the wife's s2000 and am waiting on a set for the cr-v. They even sent me a new driver's side mat for the s because the badge was upside down!
Have a set waiting for mine, ordered a set for the wife's s2000 and am waiting on a set for the cr-v. They even sent me a new driver's side mat for the s because the badge was upside down!
I have to say, the checker pattern has grown on me. The manufacturing quality isn't perfect, but for the price these mats are pretty good. I'm going to look into adding hooks to the carpet so they don't slide up as much.
Awhile back I contacted the company about the driver's side being short, and they were going to send me an updated set (I provided them new measurements), but they've not responded since so I'm thinking it's not going to happen.
I have to say, the checker pattern has grown on me. The manufacturing quality isn't perfect, but for the price these mats are pretty good. I'm going to look into adding hooks to the carpet so they don't slide up as much.
Awhile back I contacted the company about the driver's side being short, and they were going to send me an updated set (I provided them new measurements), but they've not responded since so I'm thinking it's not going to happen.
Chances are they don't manufacture them, they just get what they get. Only reason I got a replacement was a build error.
I think P2M does manufacture them, I bought them through an eBay store, but he contacted P2M on my behalf about the mat length.
Its the driver's side, from the bottom edge nearest the seat mount to the seat mount itself, I have some 5" of space.
Mine were from an eBay store as well. Circuit spec something or other. They were pretty helpful.
I went and crawled under the plastic to get a couple of pics, here's the driver's mat. Seems like it's correct to me. The could be a bit longer but it will still sit under the pedals.
I think on mine the curved area by the trans tunnel is further up, so if I pull the mat that far back then the curve doesn't line up anymore... Maybe they did end up taking my measurements and making a change? I'll have to go out and grab some pics when I get a chance.
Speaking of carpets, I see you have the ACC carpet. How was fitment for you? I had lots of trouble with the molded seat mounts not being deep enough. I like that you have the loop-style one though. I have the plush cut-pile version, which is fine, except it tends to hold pine needles and other debris more easily.
I think on mine the curved area by the trans tunnel is further up, so if I pull the mat that far back then the curve doesn't line up anymore... Maybe they did end up taking my measurements and making a change? I'll have to go out and grab some pics when I get a chance.
Speaking of carpets, I see you have the ACC carpet. How was fitment for you? I had lots of trouble with the molded seat mounts not being deep enough. I like that you have the loop-style one though. I have the plush cut-pile version, which is fine, except it tends to hold pine needles and other debris more easily.
Also, you have quite the wiring job ahead of you.
fits like you'd expect. without the oem foam its loosearound the tunnel. i prefer that to old and gross.
that wiring will mostly be ripped out. on top of the elite 1500 and ic7 dash i ordered the PD16 power delivery to replace the factory fuse panel. it will go in the rear cubby and everything will run to there instead of under the dash. wiring is my happy place.
everything on the car kind of just works as it should
When will I learn to stop saying these things?
Leaking right out of the tie rod boot. Maybe I cracked a seal when I rebuilt it 2+ years ago and it just didn't give out until now? Going to price out having someone rebuild it, otherwise I'll grab a kit and do it again myself.
And right after my exam season ended too. Oh well, what can you do.
Pulled the steering rack today. I don't have the kit to rebuild it yet, but it's a nice day out. Pulling it was fairly straightforward; wheels and undertray out:
Then I decided to remove the inner tie rods while the rack was still in the car. You could remove the rack as a unit, but this gave me more leverage to crack them loose. Right side was full of ATF:
Left side full of grease, and surprise, also ATF. I'm guessing the seal that failed is the inner one between the piston side of the rack and the grease side of the rack. I remember when installing that I had to very carefully work that seal over the teeth on the rack, and I was certain I had done it without damage. I guess I was wrong.
This is the sludge that came out of the rack:
I also noticed something a bit weird. When I got in the car I realized that there were fewer turns to lock right than there were left. So I made a point of measuring when I took the boots off:
This is the passenger's side. Driver's side not photographed due to difficulty getting the shot, but I measure 2" there. This means that the rack is offset 1/2"" to the right. Is this normal? Did the alignment shop just not catch it? I kept the inner and outer rods together in the same position they were removed, so when I reinstall the rack I am going to center it with the ruler and then take out the 1/4" on the passenger's side rod and add it to the driver's side. I'm guessing there must be some margin for error in this, but 1/2" seems like a lot.
Then I cracked all the hoses loose and let them drain into a pan. Six bolts hold the rack on the sub-frame, but the impact made quick work of it. Then after one bolt on the steering column the rack was free. Actually getting it out of the car required that I loosen the sway bar and remove some other things for clearance:
With the electric fan out, the rack can be rotated out with some care. I'm guessing on a stock car you don't need to remove the fan and shroud, but the Taurus electric fan takes just enough space to make it necessary.
Then I put everything I removed in the garage, and it will sit there while I patiently wait for the rebuild kit.
ETA is Monday, but I won't have time to do the rebuild for a few days thereafter. On a side note, I also noticed a bit of glitter in some of the ATF I drained. I don't know what would cause that (there is no metal to metal contact in the ATF side of the rack, and there was plenty of grease on the rack/pinion side) but it's concerning. I added some fluid to the pump reservoir and spun it with the electric impact (low speed), and the fluid that came out was clear of debris. I won't know until I break down the rack.
when you put it back together go from lock to lock with the steering wheel, and then go back half way. or its like 3 turns lock to lock, so turn it to lock, and then 1.5 turns back, and its centered.
ive heard horror stories about doing steering racks on other cars, but the FC is so easy, Mazda must have heard some of those stories too
ive heard horror stories about doing steering racks on other cars, but the FC is so easy, Mazda must have heard some of those stories too
I did the lines on my Celica (not even the rack itself, just lines) and the rack is sandwiched between the engine and the firewall. Doing just the lines was a multi-day job, requiring a Sawzall to get the old lines out, and only one wrench fit in the available space, so I had to use both a wobble-joint and crows-foot socket to tighten the new ones. Even then the fitting only turned like 15° at a time, so it was at least 25-30 minutes just getting one fitting tightened down.
If I have to remove the actual rack one day, I'm just going to pull the engine and trans to save myself time. Mazda spoiled us making the Rx7 this simple to work on.
I don't think I really documented my steering rack rebuild last time, so this time I made sure to take some pictures. I remember this process being really intimidating last time, but this time it went smoothly. There really aren't that many parts to deal with; you just need to make sure you remember where they go and take care not to damage any of the parts.
The seal kit arrived while I was at work today and I found some time after for the tear-down and cleaning. First comes the removal of the yoke support and the bottom pinion bearing cover (I made up the name, I don't know what the real term is). If you've been reading the past few posts you're more than familiar with the yoke support, but the bottom pinion bearing cover is a 24mm nut on the bottom of the rack. Look under it and you find:
The bottom pinion bearing; what else? Also though, you do find a 17mm nut that you definitely tightened before assembly but is now floating around loose on the threads. I distinctly recall torquing this to spec and now it's completely loose, so maybe some blue loctite is in order this time. Although it may be the fault of the bearing somehow, since this one is toast. Spinning it around has that distinct "crunchy" feelings that bearings get when it's time for them to go to the big toolbox in the sky.
The part number is Koyo 6001. I found a compatible part on Amazon with next-day delivery, 10 pack for $15. Generally I just prefer to buy Koyo / Timken the first time, but at that price I decided to just roll the dice. So much like those ball-bearings for the yoke support, if anyone needs a bottom pinion bearing, just let me know.
Next I took off a dust cover and snap-ring on top of the pinion. Then you can take the pinion assembly out by gently tapping on that bottom nut until it's loose in the housing, and removing the nut before pulling it all the way out:
The top bearing and bottom oil seal came out with it, which is normal. This part does the "magic" in a power steering rack. When you are turning left it pressurizes the one side of the piston and pushes the rack left, while allowing fluid out from the other side of the piston (through those hardlines). When turning right, it pressurizes and de-pressurizes the opposite sides and turns right. This way the pressurized ATF does the work for you, which is pretty nifty. Now that's my layman's understanding, and there are also some wacky things going on with the third line for the "reaction force" tube that I don't entirely understand. Basically it seems like that line senses how much pressure is opposing the turning motion of the tires (basically whether there is significant resistance like hot asphalt, or little resistance like snow) and does something with the valve in the pump to better react to road conditions. Again, layman's understanding.
Then I removed the hardlines from the back of the rack. They run from the pinion housing to the ATF side of the rack, and are what carries the actual pressurized fluid to press on the piston and move the rack. Next you need to remove the rack stopper:
A screwdriver fits through those notches, then you rotate the little steel wire out of it's groove. Then the stopper pops out. After the stopper is removed, there is a fluid seal that sits inside a steel bushing, with an o-ring on the outside to seal against the tube. This is removed by gently tapping on the gear side of the rack with a dead-blow hammer and extension, basically using that piston on the rack itself to gently push the bushing and seals out. Then the rack is free:
Then I used a 19mm socket and multiple extensions as a dead-blow hammer to remove the inner ATF seal and it's support piece:
This is the seal I mentioned before that is tough to install. It needs to slide over the toothed side of the rack, so it's easy to snag it and crack the plastic insert. I was 100% sure I got this right last time (practiced with the old seals a few times too), but it's clearly cracked. At least I have a likely culprit for the failure.
The last step is to remove the bottom pinion bearing. A socket and hammer (noticing a theme here?) made quick work of it. Note that a puller (blind-hole puller?) is the correct tool, but I don't have one. There is also a Mazda SST for the inner seal and support I mentioned above, but I don't have that either and the bearing & extensions work just fine as long as you take care with it.
After that it's time to clean everything very, very thoroughly and inspect for damage. The rack was exactly like I remember it last time; there is only one place with any visible wear:
The flash makes them look worse than they are, but they're barely visible to the eye. I'm wondering if the passenger's side tie-rod boot was compromised before I bought the car. There are no tears in it now, but it may have been replaced before.
I tried and couldn't feel anything that I could catch a nail on. With little else to go on (there is no procedure in the Factory Service Manual on what the acceptable wear is or how to measure), I'm using that as my barometer and calling it fine. Anything I do to try and improve it is liable to make it worse, so it's staying as it is.
This is the best picture I could get, but there is one more bearing we need to concern ourselves with:
Don't damage that needle bearing! Apparently Mazda doesn't acknowledge the part at all, it has no part number in the microfiche, and it's a non-standard side making it difficult to find a replacement. Let alone actually getting the old one out and the new one in. Thankfully mine is nice and smooth, so I don't have to worry about it.
Next I got the inside of the rack squeaky clean. Photographing this is a challenge, so this is the best I've got for you:
It's super smooth, so it looks like it's in good shape for the rebuild. Copious amounts of brake cleaner and a blue shop rag on a stick took care of the cleaning.
And the last part of note; one of the old seals on the pinion. There are four of these, and they are the least flexible seals I've ever seen. Take care not to break them when installing. This is one of the old ones I pulled out, and that is NOT the side I used the pick on to remove it. That was already there. And I definitely didn't assemble the rack with it damaged. I can only assume that either I snagged it on the install, or it was otherwise compromised and then the loose nut on the bottom of the pinion allowed it to wobble and wear down. The pinion, however, shows no signs of unusual wear or contact with the housing. To sum up: It's almost certainly something I did wrong, I just don't know exactly what.
Lastly, here's a photo of all the cleaned pieces. It took an hour at least, but they are all clean of grease now:
Please ignore my very messy workbench and the surrounding detritus. You can also see some marks on the back of the toothed portion of the rack. These are from driving around without that ball-bearing for awhile, but are just some light marks and won't affect operation of the rack and pinion. That part of the rack doesn't see ATF, only grease, and is only sealed by the dust-boot. After all that work cleaning, I immediately undid it by covering everything with a light coating of ATF. Rust never sleeps.
The bearing should arrive tomorrow, and I'm going to pick up some paint to make this look a lot nicer. I'm thinking I'll remove all the paint from the aluminum pinion housing and leave it bare, then get some satin black for the ATF side of the rack since it's steel. If all goes well the update should be soon and hopefully the rack is back in by Wednesday.
In other news, I was working on the brake lines near the master cylinder and when bleeding the brakes afterwards the rear left soft-line started to leak from the fitting. Not the fitting where it meets the hard-line, the actual crimped connection. Yikes. I've put in an order through Mazdatrix, and though my wallet hurts ($90 USD for the lines, $45 USD flat rate shipping to Canada, then exchange, and customs is inevitably going to rub salt in the wound), I know these lines are DOT approved and should last a long time. I don't remember where exactly I got the old braided stainless lines, but they clearly weren't good enough and I'm glad it failed in the driveway instead of on the road.
The bearings came in from Amazon as expected, so having everything I needed I rebuilt the rack today. Reassembly is more or less the reverse of disassembly. In fact, the job really only takes about an hour, but this turned into about 6 hours because I decided to worry about the cosmetics. I ended up using a wire-wheel on an air die-grinder to remove all the paint from the pinion housing, to the right of the mount. Then I cleaned and scuffed the rest of the rack before painting with VHT satin black chassis/roll bar paint. I've used the gloss version before and it's super tough stuff, so hopefully the satin is tough as well. The hardlines and mounts got the same paint. Photos of that to come, but first the mechanical bits.
The inner seal goes on over the teeth as I mentioned, which is the seal you need to be super careful not to damage. Then the little steel collar goes on with it, and the blue o-ring goes on the piston:
I noticed something interesting about the green seal though. Notice the following, and keep in mind this is the NEW seal:
Yup, they all have that notch. I checked both old ones and both new ones, they're identical. This means I didn't screw it up last time. Maybe the o-ring on the control valve was the culprit all along, and the shaft seals started leaking from over-pressure or something.
Anyways, the next step is to put in the rack, then use the geared end to bang the inner seal and metal collar into place. That Mazda SST is probably a more elegant solution, but this works:
Next I dealt with the bearing. The ones from Amazon have identical dimensions:
It's a sealed design, but in this application I don't see that making any difference.
Like I said, if anyone needs a bearing just let me know. I have 9 spares...
To install it, I just tapped it into place with a 21mm socket and the dead-blow hammer:
With that in place, I put the new rack seal and o-ring into the little carrier and installed it onto the passenger side of the rack:
Carefully popped that in. Then installed the rack stopper and made sure it seated completely, before winding in the wire retainer:
With that done, it was time to turn to the pinion and control valve. Not photographed, but I greased the needle bearing in the housing before installation. I put lots of grease on the pinion itself, and the control valve has new seals with lots of ATF. These are the least flexible o-rings I've ever encountered, so they need a lot of care to avoid damaging them:
Then after installing the pinion and making sure it was aligned, I installed the bottom lock-nut and torqued to the factory 22 ft-lbs:
To get the grease all the way into the rack, I slapped it onto the toothed section and then wound the rack back and forth a few times. This way I know it's all well lubricated:
I then had to improvise a solution for a slightly unusual problem. The ball-bearing I used in the support yoke cracked the hole in the yoke itself, and popped through to the other side. I've mentioned before that this part is NLA.
I first tried just putting a bead of weld on the back side, but that burned through immediately even on the lowest setting. So then I went to my second option, which was to drill out the hole very slightly and use the 5.5mm ball bearing I got on eBay with the others:
And well, it works fine. The ball-bearing spins easily in the cradle. Later when I installed the support I was able to torque it to spec, no issues. I did notice something interesting in the training manual though; It's only the manual rack that is depicted with the ball-bearing. The power rack doesn't specifically show a ball-bearing there (although the angle from which the diagram is drawn may just obscure it). Later on the manual rack shows a transparent section on the yoke so we can see the ball-bearing in the bottom. I also found a rebuild guide on another forum with lots of photos, and I'm not 100% sure due to photo quality, but I'm fairly certain he didn't have a bearing in the yoke.
This makes me wonder if mine is supposed to not have the bearing at all, and the issues I was having were due to the pinion bearing. Maybe Mazda uses the same part for both racks but only installs the ball-bearing on the manual rack, which is why my yoke has the little cradle for it. For now it seems to torque up fine with the ball-bearing, so I'll leave it. I can always access the part later when it's in the car if I want to remove the ball-bearing.
Next I installed the upper oil seal and snap ring:
Then on goes the dust seal:
After that I installed and torqued up the yoke adjustment and the bottom pinion plug. Both were painted with the same satin black paint; I prefer the bare metal look, but they are steel and the coating had worn away, so it wouldn't be pretty for long before rust took hold:
The bottom plug got some RTV so grease doesn't find it's way out, and also because it's staked from the factory and I don't want to restake it. There is nothing on the yoke adjustment other than a bit of anti-seize.
Concurrently with the above work, I was preparing the mount brackets. I forgot to take a proper before picture, or even a proper during picture, but here's my simple electrolysis bath:
It's simple and works really well. I originally had these brackets in silver (Duplicolor engine enamel), but it really wasn't sturdy enough for the application and was flaking off. After stripping the old paint and a few hours of electrolysis, they were ready for the new paint:
And that about wraps up the day's work. After all was said and done, the rack rebuild is about complete:
I ended up painting the mount on the right even though it's part of the pinion housing, just to save myself the extra 45 minutes with the wire-wheel removing the paint from the mount. It's not show-car quality, but it's certainly better than before and it's good enough for me. The tie rods from both sides have been taken apart, boots cleaned and inspected, and prepared to be reinstalled. I am going to wait until the rack itself is back in the car to do so, since it makes the installation much easier.
And that's it for today. I have some other things to get done and it's raining out, so the re-installation will probably be tomorrow or the next day. I'm hoping to get the rack back in quickly (I may have neglected to pull my mum's NC out of the garage before taking the rack out of my Rx7, trapping it inside) and then once the brake lines arrive sometime next week I should be ready to drive it to the alignment shop. Assuming the rack doesn't explode, of course.
Forum member infernosg mentioned to me (over on Grassroots Motorsports) that he also hadn't seen the ball-bearing when de-powering his steering rack. This has turned into it's own little rabbit-hole.
FC power steering rack (from S4 training manual):
So it says something interesting, which is that the main difference in construction from the 323 / 626 is that the reaction force chamber was added. No ball-bearing depicted, no mention of it in the description.
Then the FC manual rack (same S4 training manual):
Now it specifically says that on the 323 / 626, the system has the support yoke only, and that the difference in the manual rack is the addition of the ball-bearing.
Now I tracked down a mid-80s 323 service manual and found this:
Yoke, with no ball-bearing depicted. Now my initial thinking before was that the reason the ball-bearing is not depicted separately is that it's sold with the yoke, and they just didn't think to draw it on the manual as a separate piece. Then when the yoke was NLA I couldn't confirm that hypothesis. The FC microfiche also doesn't show the ball-bearing.
Now I'm thinking that only the manual rack has the ball-bearing, and for whatever reason they chose not to install it on the power racks. I did an experiment where I removed the ball-bearing, torqued the yoke support to spec, and then tried to turn the rack by hand. I had no problem doing so. This leads me to believe the extra resistance I remedied with the ball-bearing originally was actually from something else (probably the crunchy pinion bearing). I decided to put the ball-bearing back in after seeing that the yoke wiped all the grease off the rack bar immediately, and I thought it best to err on the side of caution until I was sure.
I ended up installing the rack today (after centering the rack and correcting the tie-rod lengths to match) with no real issues. I haven't tested it with the wheels on the ground yet, but with them in the air it turned perfectly fine and was very smooth.
So I'm still waiting on those brake lines. Turned out that Mazdatrix shipped it next-day, but USPS seems to have lost it for 9 days. It went Long Beach to LA, then vanished from tracking for 9 days before appearing in Carson... 45 minutes away as Google Maps tells me. It shipped on the 2nd and only departed the airport today. Hopefully it will be here within the week, but I don't know for sure.
Until then, my Celica needed attention. If you aren't interested in Celicas then you can skip this update, the Rx7 hasn't moved since I last updated (because it has no brakes...).
I had been putting off changing to my summer wheels on my Celica because I also needed to inspect the rear brakes. This meant that if I found something wrong when taking it apart I would need to wait on parts, and then both my cars would have no brakes. But since the brake lines won't be here for awhile I decided to just risk it. For winters, I just run the stock Celica GT wheels. They were already in terrible shape when I got them, so I'm not upset by what the salt does to them:
The brake problem I was having seemed to be related to the self-adjusting mechanism on the rear drums. Basically, every few days I would notice that the hand-brake needed to be pulled harder to bite. Over time it got to the point where it didn't work at all. I had adjusted them when I installed them before the winter, but for some reason they weren't self-adjusting. After pulling them apart, my suspicions were confirmed:
On both sides, I was able to grab the drum and just pull it off. No resistance at all from the shoes. I sprayed the area down with brake cleaner but nothing seemed amiss. I know that the adjuster mechanism relies on there being contact between the shoes and drum, so I adjusted them again until I was barely able to install the drum due to resistance. Seemed to fix the problem, so I'll observe over the next few weeks for any change.
In the cabin, I needed to adjust the hand-brake at the handle. I had mitigated the problem with the parking brake by temporarily tightening the adjustment, but now the parking brake was beginning to grip up with one click. You can access it in less than one minute by popping off and rotating the shifter trim, then removing two screws and pulling out the window switch:
After backing the nut out a few threads and tightening the lock nut, it's now only three clicks to engage the hand-brake. Perfect. Then I put the summers on:
They aren't exactly my taste, but they aren't bad and they came with the car. The tires are Advan Fleva, which is nice for summer driving without wearing as quickly as grippier tires would.
With those on, I gave the car a quick wash. The paint is showing it's age in a few areas, but it still cleans up pretty nice:
I also polished the yellow out of the headlights, as I have been doing once a month since I bought the car. Before:
After:
Yes, that fender needs replacing. I think replacements are available from Rockauto, but honestly this is my daily car and it doesn't get any attention it doesn't really need.
Lastly, I found another scratch. The university parking lot has been hell for this car:
Right down through the clear into the colour... damn. Also, this car has the thinnest paint imaginable. I know the Rx7 is different since it's a transparent single-stage and lays on thicker, but I swear the paint on this Celica was allocated by the gram. Some polishing minimized the worst of this scratch:
And with that, I'm calling it a day car-wise since I head to work shortly. I still need to chase down an o2 sensor code (despite having replaced the sensor before winter), and an evap code. E-testing has been eliminated in Ontario, but there's no reason to neglect the repair. Also with the engine light on all the time I wouldn't be able to tell if a more serious code emerged.
Cleans up okay for a daily car. Hopefully the Rx7 brake lines will arrive sooner rather than later, so I can test out the steering at speed.
This is a pretty minor update overall, but I did get a little bit done on the car. When I left off I was waiting on some replacement brake lines and then an alignment. I'm happy to report the brake lines from Mazdatrix arrived and fit perfectly. Only problem is my front hardlines were seized; I was able to replace the rears no problem, but I still have the old lines in the front. Neither is leaking but since the rear one started to leak with no apparent cause or warning, I am not super confident. I will be looking into getting new lines for the front shortly, but that's on the back-burner while I deal with some other stuff.
One thing I was able to do was acquire some more OEM black interior pieces I needed. Most of them I have not had time to install, but I was able to install the sun-visors. My original visors were in very poor shape, which is why I felt perfectly fine about using the vinyl dye on them. Take a look:
The little pocket part was torn at the seam when I got the car. Multiple different glues failed to fix it. Also despite cleaning them very thoroughly before dying, the top right has an area that just turned out a bit dull. The other one is not much better. Here's what's replacing it:
Factory black piece from an S5 car. The little black clip is a 3D printed sunglasses holder. Also, check it out:
In true Mazda fashion, someone decided it was vitally important to redesign the visor clip from S4 to S5 cars. S4 on left, S5 on right. And no, they aren't interchangeable. I ended up reusing the S4 part. All installed:
There is a slight colour difference due to the dyed headliner. However the dyed headliner actually came out all one colour with no flaws, so I am perfectly content to keep it and not worry about finding the OEM black piece.
Also, I've complained about the exhaust being too loud on this car. I decided the only way to quiet it down was to add an obstruction to the exhaust stream and absorb some of that energy, so I picked something up that should help with that:
Details to come as soon as I have time. I'll be working some extra shifts for the next little bit to support my latest automotive mistake