Boost issues Fixed!
Boost issues Fixed!
So my FD (93 Touring) is stock except for M2 DP, Fluidyne Radiator, mild streetport, and slotted rotors. It was boosting 5-3-3 and after Paul at AIM tuning in Indianapolis got his hands on it, I'm boosting a perfect 10-8-10! So many things were wrong with it, I can't go into too much detail or this post would be really long.... I drove it home today and wheeeeeeeeeeeeeeeeeeeeeeeeeeeeee!!!!!! Lots o fun! Can't say enough about those guys at AIM! They are fantastic and I would highly recommend them to anyone.
please go in to detail, my friends FD is currently out of commission right now because he's boosting 10-3-3.
His mods are different, he has a 3"dp, hi-flow cat, racingbeat catback, GReddy intakes, fluidyne rad and petit AST.
Please, detail.
His mods are different, he has a 3"dp, hi-flow cat, racingbeat catback, GReddy intakes, fluidyne rad and petit AST.
Please, detail.
Joined: Aug 2005
Posts: 2,720
Likes: 1
From: Greenwood/Hartsville, SC.
Originally Posted by dgeesaman
Is your friend local? I like trying to fix boost problems.
Dave
Dave
Originally Posted by dgeesaman
Is your friend local? I like trying to fix boost problems.
Dave
Dave
If you're serious, I can PM you directions from hburg to our area.
and if you are serious, do you think you could help with his oil burning issue too? I don't mean to take advantage of your kindness at all.
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Originally Posted by FallenCho
A bottle of CD2 will help with oil burning.
Good stuff.
Good stuff.
There were several problems with lazlodawg's FD.
There were several hoses mis-routed and missing. One of the major contributors was that he had a Greddy hard pipe to the lower factory Intercooler that was installed incorrectly and had been rubbing on the crank pulley. Enough to gouge a hole in it bleeding off boost.
Plus the throttle body o-ring was missing and one of the studs was boken off there.
Pauly D
AIM Tuning
Indianapolis, IN
There were several hoses mis-routed and missing. One of the major contributors was that he had a Greddy hard pipe to the lower factory Intercooler that was installed incorrectly and had been rubbing on the crank pulley. Enough to gouge a hole in it bleeding off boost.
Plus the throttle body o-ring was missing and one of the studs was boken off there.
Pauly D
AIM Tuning
Indianapolis, IN
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