boost problem, fixed..!
Thread Starter
Joined: Jan 2002
Posts: 11,093
Likes: 2
From: Hood River oregon
I was having problems with my boost. It would shoot up to 8 PSI then fall off about 5-6000.
So I wired my twin scroll actuator open.
WOW!! just hit 10psi all the way to the redline. Good lord!
Jarrett
So I wired my twin scroll actuator open.
WOW!! just hit 10psi all the way to the redline. Good lord!
Jarrett
Good to hear that you at least know where the problen resides. BTW, I am not bringing the Rex with me to Tucson (I will be there this week) so I won't be stealing that tranny from you.
Catch you later!
PJ
Catch you later!
PJ
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Thread Starter
Joined: Jan 2002
Posts: 11,093
Likes: 2
From: Hood River oregon
Originally posted by BlackRx7
with my ported motor I get full bost by 2k but it starts fallinfg off by 5500 rpms....
with my ported motor I get full bost by 2k but it starts fallinfg off by 5500 rpms....
Just out of interest (mainly to confirm the system was working properly) I did basically the same thing, but just pulled the green actuator doover the vac hose connects to. Boost came in later, and no difference in the top end, on a stock t2 with mild exhaust. Probably old news to plenty of people, but hey
Thread Starter
Joined: Jan 2002
Posts: 11,093
Likes: 2
From: Hood River oregon
Originally posted by RexRyder
um, could u explain pls j-rat?
um, could u explain pls j-rat?
Jarrett
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