1st Generation Specific (1979-1985) 1979-1985 Discussion including performance modifications and technical support sections

good day gone bad

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Old 09-18-06, 04:16 PM
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good day gone bad

I took the car around the block after I changed the oil and spark plugs. It ran fine until I decided to give it a lil boost. It went up to 5psi and then the motor just stop running. I cranked the motor but it won't turn over. After about 5 mins. of trying to get the car started I decided to push the car home. Good thing this happened around the corner of the house. Got the car home and took out the plugs. Tried cranking the motor over again and still won't turn over. I grab my 1/2 in. rachet and 3/4 socket and stuck it on the crank pully bolt. Tried to turn it over by hand but it just won't turn. That's when I knew my motor was shot. What could have cause my motor to seized? Insufficient oil going to rotor bearings? Too much boost? I have no idea. If anyone knows why this would happen please help me out.
Old 09-18-06, 05:11 PM
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Did you try turning it backwards? Broken apex seal can stop an engine, but you can often turn them backwards, if they aren't jambed too solid.
Old 09-18-06, 05:51 PM
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pull your plugs out and see if those are still intact
Old 09-18-06, 05:56 PM
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lack of tuning caused your engine to seize.
Old 09-18-06, 06:51 PM
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Your sig doesn't say anything about your fuel system and ecu?
Old 09-18-06, 06:58 PM
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Originally Posted by rotary_sex
lack of tuning caused your engine to seize.
that doesnt make sense, even if he detonated and destroyed an apex seal, it would still spin, it just wouldnt make compression, unless it was stuck like what trochoid said.
Old 09-18-06, 06:59 PM
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That sucks. I'm sorry to hear that.
Old 09-18-06, 07:13 PM
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Home made boost controller? Time for a rebuild, which means time for upgrading, which means time for big porting...
Old 09-18-06, 07:34 PM
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man that suck idk what to tell you
Old 09-18-06, 07:56 PM
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Make sure the sump plug didn't fall out. Its possible...
Old 09-18-06, 09:52 PM
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i am running a walbro 255 fuel pump and stock s4 TII ecu w/ RB FCD. I tried turning the motor the other way and still wouldn't move.
Old 09-18-06, 10:38 PM
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Did the wheels lockup when it quit running? How high in the reves did you have it.

Stock clutch?


Possible that the clutch came apart and has it stuck.


Just a WAG.
Old 09-19-06, 12:12 AM
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I won't know until I take the motor out. I was in 2nd gear at about 3K rpm when the motor stop running. Tires locked up and it stoped running. The clutch was acting kinda strange before it happened. I might drop the tranny later on tonight just for the hell of it. I'll keep you guys posted.
Old 09-19-06, 01:02 AM
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Wedge the clutch pedal in with a 2x4 or something, then try turning the motor over again and see if it acts any differently...
Old 09-19-06, 01:51 AM
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Originally Posted by perfect_circle
that doesnt make sense, even if he detonated and destroyed an apex seal, it would still spin, it just wouldnt make compression, unless it was stuck like what trochoid said.
good point. its possible he threw to much boost at a used engine and seized a bearing somehow. mabey it was just the engines time to die. noone will know till you crack that thing open.


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