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boost issues
i just recently put 11g+ into engine work and it still isn't boosting properly... not only is it not boosting properly now the coolant buzzer goes off cause i got them to put a micro tech ecu in.. it doesnt not over heat or leak any coolant cause i just got the motor rebuilt ...
here is my mod list.. i just copied and pasted it - 5spd - Half Brigde w/ 3mm seals - Aftermarket HKS Turbo Kit t51r (rebuilt) - HKS Front-mount Intercooler Kit - HKS Hypermax Fully Adjustable Suspension (new) - ALCON (GREX) Front Caliper & Rotor Big Brake-kit - Walbro Fuel Pump (new) - 1300 cc(top) and 850 cc(side) injectors (new) - Greddy Type R B.O.V - HKS Air Filter (new) - Battery Re-located In Rear (new battery) - Stainless-Steel Exhaust Manifold & External Wastegate - Micro tech ecu (new) - A/M Radiator - A/M Stainless-steel Turbo-back Exhaust with fujitsubo muffler - A/M Engine Pulleys - A/M LSD (new) - A/M Fuel-pressure Regulator(new) - 17" Advan 3-spoke Alloys (front-225), 18" (rear-285) - Falken Azenis Tires (new) - HKS EVC III Boost Controller - HKS Turbo Timer - Greddy Gauges: Boost, Oil Temp, Oil Pressure, Exhaust Temp, Water Temp - Evolution Steering Wheel - Mazdaspeed Shift knob - A/M Pedals - A/M front bumper (new) - Cat eye signal lights (new) - Changed spark plugs(new) - replaced horn(new) - Factory dual oil coolers - abs removed properly - steal braided break lines - tinted windows (new) now i dont know if it just needs a wideband to tune it properly on the road or if the coils are to old and there dying... it ran fine on the dyno but once i went to pick it up it didnt run fine at all... i called the tuning place they said it running rich witch is why it wont boost.. i dunno :scratch: :Wconfused: i am running a really old boost controller the hks evc III it still set on the setting when it came from japan. wondering if that is the issue aswell.. |
you can always bypass the boost controller and run off the waistgate spring to see if you get a change... And why did you go with 1300 top feed injectors when you could have gotten stock ones the same size? There are bad and good things whne you replace a who bunch of things at once... the good is you have a lot of new parts..new is good.... the bad is you have a lot of new parts... anything can be the problem... Post some more info on what its doing other than its not boosting(full throttle, no boost at all, boost dies off, a little boost?) Just anything to help...and your coolant issue could be from air bubble in your system they might not have bled it correctly. Good luck
Chris |
well it creeps up to .1 bar it wants to create more boost but its like there is some thing that is giving it a hesitation i will record a video of my problem and get it up on you tube soo i can show you what i am talking about.. and i went with the 1300 cc top cause that is what he recommended with the bigger port
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