Motor went finally!
5 Attachment(s)
So after 5 years of good news I finally have some bad. Front iron cracked last week. First pass I did my famous 2nd to 1st gear shift still went 6.4 at 110mph. Log showed it was like slamming the brakes on :lol: . Second pass the clutch started slipping in 2nd thru the rest of the run, had a little break up noise going theu the traps. I think the damage was done the prior run. Oiled the track bad. Luckly not the tires too much. Got the car home and didnt know were the leak was so added some oil and it fired right up only to spit oil out the crack.
Tore it down and here are the results: |
So it shows the rotors were making contact. Front bearing doesnt look good either. Housings have marks but feel pretty smooth but have better ones I can use on the rebuild. Have to check the e shaft to see if its bent but would guess it is. Before I even tore it down Ray called it.. Said contact was made on the rotors/housings. So I need to figure out what I want to change on the next build. Since its a weekend drag car I dont believe in putting a crap ton in the build, new housings, etc... Not being cheap but too many things can kill a motor.
How offers rotor work? Want them taken down on the faces and sides. |
Roberto's machine shop in Philly, one stop shop for rotary machine work... Did you pinch any side seals with the contact? We had so much contact last year that it pinched the seal in the groove
Next best prob e&j, he does his on a cnc but regardless balanc the rotating assembly one its All clearanced |
Originally Posted by Bacon
(Post 11528623)
Roberto's machine shop in Philly, one stop shop for rotary machine work... Did you pinch any side seals with the contact? We had so much contact last year that it pinched the seal in the groove
Next best prob e&j, he does his on a cnc but regardless balanc the rotating assembly one its All clearanced |
Sorry to hear it finally broke man, hopefully you'll have it back together fast and make it a comeback. You need to buy Allen's engine if he still has it for sale.
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He sold it.
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sad to hear.
The misfire you heard going through the traps, did it sound like a machine gun? |
Damn man, just got it tuned too!
Was it just that extra 100hp on the last tune that pushed it over the top? |
Originally Posted by sleeper7
(Post 11529540)
sad to hear.
The misfire you heard going through the traps, did it sound like a machine gun? |
Sorry to hear Mike... but I'm sure you'll have it back better than before in no time..
I like Rager Manderville for balance work. |
Originally Posted by speed_nyc
(Post 11529778)
i like roger mandeville for balance work.
+1 |
Roger Manderville is good and a super nice guy, that's who did my balancing.
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Got his contact info?
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Mandeville Auto Tech
545 Buffington Rd Spartanburg, SC 29303 (864) 582-0038 |
Might look at a different material for that fitting on the front. I cracked mine in the same place. I think the fitting expanded.
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I guess if you're going to blow it up, better blow it up good.
Hope to see it up and running again soon! |
Hey Mike. Just out of curiosity, what kind of RPM did you see on the 2-1 shift? Do you feel like it was contacting before or all that damage was done on the upshift?
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Originally Posted by 13B-RX3
(Post 11533772)
Hey Mike. Just out of curiosity, what kind of RPM did you see on the 2-1 shift? Do you feel like it was contacting before or all that damage was done on the upshift?
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never mind.
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Don't hold back chuck.
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But I will be running direct fire on the next motor.
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good idear Chuck! Direct Fire is the only way to go.
Replace that fitting with something else too! |
There shouldn't be oil in that part of the motor anyhow :blush:
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Originally Posted by sk8world
(Post 11534382)
But I will be running direct fire on the next motor.
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Originally Posted by 13B-RX3
(Post 11534773)
There shouldn't be oil in that part of the motor anyhow :blush:
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