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-   -   1974 13b-re Nova (https://www.rx7club.com/old-school-other-rotary-63/1974-13b-re-nova-727207/)

13brenova 09-11-10 10:58 PM


Originally Posted by ultimatejay (Post 10211014)
Congrats on not blowing up the engine. Like what other people have said, with an experienced tuner you should get alot more power. You're still way rich at 10.5.
I didn't see it or maybe I missed it but what fuel are you using?

Sonoco 116. Wow! 12-13 afr is much leaner than I'm used to going on turbo'd piston cars. Considering the extra 20 hp we saw from the bump from 10.0 to 10.5 afr, I'd bet there would be a considerable amount of power going that lean! Looked for a good thread concerning afrs on race gas but came up nil.

Spirit-RE 09-12-10 01:53 PM

Props on an amazing build!

Erdin 09-13-10 03:51 PM

Have you had a chance to do any more tuning?

ChrisRX8PR 09-14-10 10:00 AM


Originally Posted by 13brenova (Post 10211061)
Sonoco 116. Wow! 12-13 afr is much leaner than I'm used to going on turbo'd piston cars. Considering the extra 20 hp we saw from the bump from 10.0 to 10.5 afr, I'd bet there would be a considerable amount of power going that lean! Looked for a good thread concerning afrs on race gas but came up nil.

I keep my 13B's at less than 11.5 AFR under all boost. I shoot for 11.2 and keep it between 10.8-11.5. Its pretty safe. Would not go near 12 under boost unless you are talking about 13psi or less.

Nice build.

Chris

13brenova 09-14-10 08:43 PM


Originally Posted by ChrisRX8PR (Post 10215072)
I keep my 13B's at less than 11.5 AFR under all boost. I shoot for 11.2 and keep it between 10.8-11.5. Its pretty safe. Would not go near 12 under boost unless you are talking about 13psi or less.

Pump gas or race gas?

teddyrx2 10-10-10 10:52 PM

any updates? anymore pics? run times? slips something?

ultimatejay 10-11-10 09:38 PM


Originally Posted by teddyrx2 (Post 10261770)
any updates? anymore pics? run times? slips something?

I'll let him tell you the bad news...:(

Or you can go over to the single turbo forum.

TheAbsence 10-11-10 09:58 PM


Originally Posted by ultimatejay (Post 10263597)
I'll let him tell you the bad news...:(

Or you can go over to the single turbo forum.

https://www.rx7club.com/single-turbo-rx-7s-23/blew-engine-need-help-diagnosing-924962/

NOOOOOO!

13brenova 10-13-10 08:17 PM

Yep. It's true......popped the motor. On the first cool day of fall, I took it out for a run and the boost hit 27 psi instead of the previous 22 psi. A number of things lead to it's demise, but two of the major contributors were too hot of a plug with too large of a gap coupled with a week ignition.

No worries though, I planned on toasting at least one motor in the learning process. Gives me time to finish the lingering things on the car in the meantime.

When the engine let go.........that fucker was straight out flying!

teddyrx2 10-13-10 09:18 PM

that sucks bro...

JS88 10-25-10 10:49 AM

Great car, really impressive. Good luck with the new motor!

13brenova 10-27-10 08:22 PM

4 Attachment(s)
Well, the revival begins. Sending the turbo to A-Spec for inspection and a swap from the 1.15 ar turbine housing to a 1.01. The new 4.30 back cut gears came in from Moser to replace the original 4.88 gears. These two things should help the boost come in a little bit quicker. Going to finish the windows, chassis wiring, and some other pending items before pulling the engine for a rebuild.

In the meantime, I finished the new driveshaft loop.

teddyrx2 10-28-10 04:29 AM

beautiful bro...

Frankenrex 10-28-10 10:48 PM

That has got to be the nicest looking driveshaft safety hoop I've ever seen...

13brenova 12-11-10 09:51 AM

4 Attachment(s)
A little more progress. I decided to add loops to the front and rear of the car to hook to for dyno runs, strapping the car on the trailer, and towing the car when the engine blows. :lol: When we took the car to the dyno, they screwed up the paint on the axle and scuffed the finish on the gas tank. Kind of pissed me off, so I came up with these. Pics of the front to come....

13brenova 12-11-10 10:00 AM

4 Attachment(s)
Also finished the windows and door panels. I made the drivers side removable so I can still get out of the car when it's in an enclosed trailer.

13brenova 12-11-10 10:01 AM

1 Attachment(s)
The new ECU also came in.

BUMBLEBEE7 12-11-10 10:34 AM

Is the new motor ready? I hope the Haltech meet the needs of your set up. Keep up the GREAT work!

ultimatejay 12-11-10 04:30 PM

Nice. So who's going to make the first 1/4 mile pass... you or Allen? :lol::lol::lol:

rex3 12-11-10 07:53 PM

My goodness... I must say you are one hell of a fabricator. This is a badass build.

13brenova 12-11-10 09:53 PM


Originally Posted by ultimatejay (Post 10362058)
Nice. So who's going to make the first 1/4 mile pass... you or Allen? :lol::lol::lol:

I've got money on Allen!:nod:

13B-RX3 12-19-10 11:12 PM

March is right around the corner!!! You better get cracking!

teddyrx2 12-22-10 03:27 AM

I like the strap/tow hooks that nice and different at the same time...

what up allen whats good bro...

13B-RX3 12-22-10 10:45 AM

Not much Teddy, just trying to make a living!

F1ashpoinT 12-27-10 02:49 PM

This is really unique, I love it.

oldschoolbaby 12-29-10 01:57 AM

There goes an awesome looking Nova, damn thats fast! wait, that doesnt sound right... brap-brap-brap-brap... heeehaaa!!! Awesome car!

13brenova 12-31-10 05:57 PM

5 Attachment(s)
With the big ACT single plate clutch, you had to be the leg squat king to push in the clutch. So, I made a new master cylinder bracket to allow me to move the hole further up on the clutch pedal to give a better pedal ratio. While I was at it, I made a bracket for a clutch switch to activate the no-lift shift and anti-lag/aux rev limit for launching. I had a hydraulic switch before, but sometimes it would trigger the no-lift shift during non-power shifts due to the restrictor oriface in the clutch line I am using to ease the shock on the drivetrain. The new software with the PS1000 would have fixed the problem, but I like this switch setup better.

Now, onto the engine...........

13B-RX3 01-02-11 07:17 PM

Nice as always Nick. Now quit fucking with that little shit and get that motor out!!!

13brenova 01-02-11 07:42 PM


Originally Posted by 13B-RX3 (Post 10394666)
Nice as always Nick. Now quit fucking with that little shit and get that motor out!!!

Working on it right now.........beotch!!!!!!:lol:

13B-RX3 01-02-11 08:43 PM

Details!!!!!!!!!!!!!!!!!!!

13brenova 01-02-11 08:57 PM


Originally Posted by 13B-RX3 (Post 10394810)
Details!!!!!!!!!!!!!!!!!!!

Everything is disconnected and the engine will be out by 10am tomorrow. I think I am going to send the engine somewhere for the rebuild. We've gotta get the solid axle conversion done on the vette, and I don't think I'm going to have time to do the engine myself. So, while the engine is being rebuilt, we'll do that project and be ready to reinstall the engine when it returns. After that, the only thing I need to do is a couple of wiring changes I want to do for the PS1000.

I'll call you tomorrow afternoon.....

13brenova 01-03-11 09:15 PM

5 Attachment(s)
Got the engine pulled. I also managed to get the front tow hooks welded in.

teddyrx2 01-04-11 04:36 AM

its the small details like that,,, that make the car stick out and look so much better...you got skills bro...

Erdin 01-29-11 02:06 PM

any updates?

Chuck Norris FB 01-29-11 04:37 PM

^^ What he said:beard:

13brenova 02-02-11 08:19 PM


Originally Posted by Erdin (Post 10442398)
any updates?

Pineapple Racing has the engine and Rob tore it apart yesterday. Rear rotor and housing are toast, but everything else looks great. He said there is no real indication of where the coolant leak or oil consumption was coming from so he's looking into it further. He also said that the apex seals craking didn't look like it was from detonation as the rear rotor isn't dented at all. He is leaning toward a flame front problem either from bad gas or possibly too retarded timing like Alan and others have eluded to. He should have things back together shortly. He was also pretty impressed with the oil pan. Everything else is ready to go once the engine arrives.

In my quest to have the lightest clutch pedal in the world on an ACT Extreme Pressure plate, I found a 7/8" slave cylinder instead of the stock 3/4" bore I had. I have plenty of pedal travel to accomodate, so I think it will work well. My brother machined it to fit on the TII transmission for me.

In the mean time, we are converting the old man's '69 vette to a 4-link and Ford 9" with a 598 cid Shafiroff engine. I still talk shit to him and tell him the nova is going to kick his vette's ass. Not true, but I have him convinced it will :egrin:.

13brenova 02-02-11 08:26 PM

Oh yeah....my wife put together a video of the Nova too. You guys have seen all of the stuff before, but it's kind of cool to watch and not have to look through 22 pages of posts to see the build.

http://www.youtube.com/watch?v=-SBpIwKfjps

1BADSP 02-02-11 09:03 PM

It was cool to see that oil pan,I watched rob take your engine apart,I didn't know it was yours until reading your last post.your engine is in the best of hands.he will be teaching me to tune on my turbo RX-3 soon.

ultimatejay 02-02-11 11:57 PM

Nice vid.

Erdin 02-03-11 04:15 AM

robs a good man, your in good hands:)

dekam 1 02-03-11 11:29 PM


Originally Posted by 1badsp (Post 10450539)
it was cool to see that oil pan,i watched rob take your engine apart,i didn't know it was yours until reading your last post.your engine is in the best of hands.he will be teaching me to tune on my turbo rx-3 soon.

yes sir the motors is in good hands. Rob makes the trip over to hawaii to help with my race car. In the 3 years of his trips here, ive learned much. He has never steared me wrong in reaching my racing goals as we have meet all of them so far. Rob will do the motor right

dekam 1 02-09-11 07:08 PM

any updates on motor?

13brenova 03-21-11 08:08 PM

5 Attachment(s)
The carnage...........how in the hell did the turbine wheel not get a scratch?

Attachment 719966

Attachment 719967

Attachment 719968

Attachment 719969

Attachment 719970

13brenova 03-21-11 08:15 PM

1 Attachment(s)
:egrin:

Same setup as before, but with 3mm Hurley's this time. Rob did a little cleanup on the portwork as well.

Attachment 719971

Narfle 03-21-11 09:07 PM

Awesome. Don't overboost this one!

13brenova 03-21-11 09:25 PM

I'd say I won't..........but I will. As long as it's intentional this time!!!!

cfamilyfix 03-21-11 10:38 PM

The car and the motor are beautiful! I think this thing is screaming for a 20b. The torque numbers alone warrant the build. Maybe the next engine??? Again...your work is outstanding. Can't wait to see how this motor runs.

13B-RX3 03-22-11 01:11 AM

Looking good Nick! Now throw that bitch in and lets go!!!

13brenova 05-08-11 09:01 AM

She's back under her own power now.

http://www.youtube.com/watch?v=0ftcUKaCdnc

Just have to do a little machining to get the crank trigger working in place of the CAS and then I'm ready for the Florida trip with Allen to get this thing tuned.

13brenova 05-08-11 10:02 AM

We never really came to a consensus as to why the first engine blew. Obviously it had to do with the boost spiking up to 27 psi due to denser air on a cool day, but the car was running Sonocco 116 and the afrs were right at 11.0. If everything else was correct, the engine should have been able to handle this. So, I tried to address everything that could have lead to the previous enigne's demise.

- 3 mm Hurley seals vs the previous 2mm Mazda seals. Hopefully they will be a little more detonation resistant

-MSD LS1 coils replace the stock LS1 coils on the leading plugs. The trailing coils are intentionally still the stock LS1's so they are a lower energy. (I'm pulling this out of my ass....so bare with me) Things could have possibly gone awry if the leading plug started to misfire at higher boost, causing the trailing plug to light the mixture later in the cycle. Then the extremely high exhaust temps caused by the late ignition of the mixture could have ignited the intake charge due to the overlap from the bridgeport.

-Plugs have been changed from BUR9EQ's all the way around to 10.5 race plugs on the leading and 11.5 race plugs on the trailing. There is a possibility that the BUR9EQ's were too hot of a plug (especially on the trailing) and lead to preignition.

-Haltech e8 has been replaced with the new PS1000. At the instant the engine blew, the data log dropped out for a second or two and then restarted. Haltech said that this was due to the large amount of electrical noise created by the massive misfiring when the engine blew. It still sits in the back of my mind that maybe the "glitch" that happened the instant the engine blew was the cause instead of the result. Anyway....the PS is supposed to be much more resistant to noise and has much better software that includes "engine protection".

-The overboost protection in the Haltech is now configured and active.....no explanation needed :lol:

-Allen thinks that the most likely reason the engine went "boom" was due to extremely conservative timing resulting in high EGTs and ignition of the intake charge. Hence the trip to let the pros tune this time.

-The previous gas I was using was Sonocco 116 supplied by a local performance shop. This is one of those deals where it is transferred from a drum to my container. I can't be a hundred percent sure that the guy pumping didn't get things mixed up and give me the wrong gas. So from now on...........C16 from sealed 5 gallon containers, direct from VP.

- The CAS is being replaced by a Full Function Trigger wheel with a Hall Effect sensor just in case the CAS signal got a little flakey causing the engine to pop. Anything that is more resistant to noise and gives a more stable timing signal is all good in my book. Should have the necessary parts machined to adapt their kit to my gilmer pulley this week.

- EGTs are now being logged in the Haltech. I didn't have this working during the previous dyno runs and might have been able to see that something wasn't quite right prior to the engine letting go. When the engine popped, it was the first run with the EGT's being logged, and by that time, it was too late.

-EGTs in the rear rotor were slightly higher than the front, so now I am running 2% more fuel on the rears vs the front to even them out a bit.

Let's hope the changes pay off. If they don't.....the new tow hooks will!


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