Originally Posted by ultimatejay
(Post 10211014)
Congrats on not blowing up the engine. Like what other people have said, with an experienced tuner you should get alot more power. You're still way rich at 10.5.
I didn't see it or maybe I missed it but what fuel are you using? |
Props on an amazing build!
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Have you had a chance to do any more tuning?
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Originally Posted by 13brenova
(Post 10211061)
Sonoco 116. Wow! 12-13 afr is much leaner than I'm used to going on turbo'd piston cars. Considering the extra 20 hp we saw from the bump from 10.0 to 10.5 afr, I'd bet there would be a considerable amount of power going that lean! Looked for a good thread concerning afrs on race gas but came up nil.
Nice build. Chris |
Originally Posted by ChrisRX8PR
(Post 10215072)
I keep my 13B's at less than 11.5 AFR under all boost. I shoot for 11.2 and keep it between 10.8-11.5. Its pretty safe. Would not go near 12 under boost unless you are talking about 13psi or less.
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any updates? anymore pics? run times? slips something?
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Originally Posted by teddyrx2
(Post 10261770)
any updates? anymore pics? run times? slips something?
Or you can go over to the single turbo forum. |
Originally Posted by ultimatejay
(Post 10263597)
I'll let him tell you the bad news...:(
Or you can go over to the single turbo forum. NOOOOOO! |
Yep. It's true......popped the motor. On the first cool day of fall, I took it out for a run and the boost hit 27 psi instead of the previous 22 psi. A number of things lead to it's demise, but two of the major contributors were too hot of a plug with too large of a gap coupled with a week ignition.
No worries though, I planned on toasting at least one motor in the learning process. Gives me time to finish the lingering things on the car in the meantime. When the engine let go.........that fucker was straight out flying! |
that sucks bro...
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Great car, really impressive. Good luck with the new motor!
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Well, the revival begins. Sending the turbo to A-Spec for inspection and a swap from the 1.15 ar turbine housing to a 1.01. The new 4.30 back cut gears came in from Moser to replace the original 4.88 gears. These two things should help the boost come in a little bit quicker. Going to finish the windows, chassis wiring, and some other pending items before pulling the engine for a rebuild.
In the meantime, I finished the new driveshaft loop. |
beautiful bro...
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That has got to be the nicest looking driveshaft safety hoop I've ever seen...
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A little more progress. I decided to add loops to the front and rear of the car to hook to for dyno runs, strapping the car on the trailer, and towing the car when the engine blows. :lol: When we took the car to the dyno, they screwed up the paint on the axle and scuffed the finish on the gas tank. Kind of pissed me off, so I came up with these. Pics of the front to come....
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Also finished the windows and door panels. I made the drivers side removable so I can still get out of the car when it's in an enclosed trailer.
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The new ECU also came in.
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Is the new motor ready? I hope the Haltech meet the needs of your set up. Keep up the GREAT work!
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Nice. So who's going to make the first 1/4 mile pass... you or Allen? :lol::lol::lol:
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My goodness... I must say you are one hell of a fabricator. This is a badass build.
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Originally Posted by ultimatejay
(Post 10362058)
Nice. So who's going to make the first 1/4 mile pass... you or Allen? :lol::lol::lol:
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March is right around the corner!!! You better get cracking!
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I like the strap/tow hooks that nice and different at the same time...
what up allen whats good bro... |
Not much Teddy, just trying to make a living!
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This is really unique, I love it.
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There goes an awesome looking Nova, damn thats fast! wait, that doesnt sound right... brap-brap-brap-brap... heeehaaa!!! Awesome car!
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With the big ACT single plate clutch, you had to be the leg squat king to push in the clutch. So, I made a new master cylinder bracket to allow me to move the hole further up on the clutch pedal to give a better pedal ratio. While I was at it, I made a bracket for a clutch switch to activate the no-lift shift and anti-lag/aux rev limit for launching. I had a hydraulic switch before, but sometimes it would trigger the no-lift shift during non-power shifts due to the restrictor oriface in the clutch line I am using to ease the shock on the drivetrain. The new software with the PS1000 would have fixed the problem, but I like this switch setup better.
Now, onto the engine........... |
Nice as always Nick. Now quit fucking with that little shit and get that motor out!!!
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Originally Posted by 13B-RX3
(Post 10394666)
Nice as always Nick. Now quit fucking with that little shit and get that motor out!!!
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Details!!!!!!!!!!!!!!!!!!!
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Originally Posted by 13B-RX3
(Post 10394810)
Details!!!!!!!!!!!!!!!!!!!
I'll call you tomorrow afternoon..... |
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Got the engine pulled. I also managed to get the front tow hooks welded in.
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its the small details like that,,, that make the car stick out and look so much better...you got skills bro...
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any updates?
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^^ What he said:beard:
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Originally Posted by Erdin
(Post 10442398)
any updates?
In my quest to have the lightest clutch pedal in the world on an ACT Extreme Pressure plate, I found a 7/8" slave cylinder instead of the stock 3/4" bore I had. I have plenty of pedal travel to accomodate, so I think it will work well. My brother machined it to fit on the TII transmission for me. In the mean time, we are converting the old man's '69 vette to a 4-link and Ford 9" with a 598 cid Shafiroff engine. I still talk shit to him and tell him the nova is going to kick his vette's ass. Not true, but I have him convinced it will :egrin:. |
Oh yeah....my wife put together a video of the Nova too. You guys have seen all of the stuff before, but it's kind of cool to watch and not have to look through 22 pages of posts to see the build.
http://www.youtube.com/watch?v=-SBpIwKfjps |
It was cool to see that oil pan,I watched rob take your engine apart,I didn't know it was yours until reading your last post.your engine is in the best of hands.he will be teaching me to tune on my turbo RX-3 soon.
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Nice vid.
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robs a good man, your in good hands:)
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Originally Posted by 1badsp
(Post 10450539)
it was cool to see that oil pan,i watched rob take your engine apart,i didn't know it was yours until reading your last post.your engine is in the best of hands.he will be teaching me to tune on my turbo rx-3 soon.
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any updates on motor?
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The carnage...........how in the hell did the turbine wheel not get a scratch?
Attachment 719966 Attachment 719967 Attachment 719968 Attachment 719969 Attachment 719970 |
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:egrin:
Same setup as before, but with 3mm Hurley's this time. Rob did a little cleanup on the portwork as well. Attachment 719971 |
Awesome. Don't overboost this one!
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I'd say I won't..........but I will. As long as it's intentional this time!!!!
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The car and the motor are beautiful! I think this thing is screaming for a 20b. The torque numbers alone warrant the build. Maybe the next engine??? Again...your work is outstanding. Can't wait to see how this motor runs.
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Looking good Nick! Now throw that bitch in and lets go!!!
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She's back under her own power now.
http://www.youtube.com/watch?v=0ftcUKaCdnc Just have to do a little machining to get the crank trigger working in place of the CAS and then I'm ready for the Florida trip with Allen to get this thing tuned. |
We never really came to a consensus as to why the first engine blew. Obviously it had to do with the boost spiking up to 27 psi due to denser air on a cool day, but the car was running Sonocco 116 and the afrs were right at 11.0. If everything else was correct, the engine should have been able to handle this. So, I tried to address everything that could have lead to the previous enigne's demise.
- 3 mm Hurley seals vs the previous 2mm Mazda seals. Hopefully they will be a little more detonation resistant -MSD LS1 coils replace the stock LS1 coils on the leading plugs. The trailing coils are intentionally still the stock LS1's so they are a lower energy. (I'm pulling this out of my ass....so bare with me) Things could have possibly gone awry if the leading plug started to misfire at higher boost, causing the trailing plug to light the mixture later in the cycle. Then the extremely high exhaust temps caused by the late ignition of the mixture could have ignited the intake charge due to the overlap from the bridgeport. -Plugs have been changed from BUR9EQ's all the way around to 10.5 race plugs on the leading and 11.5 race plugs on the trailing. There is a possibility that the BUR9EQ's were too hot of a plug (especially on the trailing) and lead to preignition. -Haltech e8 has been replaced with the new PS1000. At the instant the engine blew, the data log dropped out for a second or two and then restarted. Haltech said that this was due to the large amount of electrical noise created by the massive misfiring when the engine blew. It still sits in the back of my mind that maybe the "glitch" that happened the instant the engine blew was the cause instead of the result. Anyway....the PS is supposed to be much more resistant to noise and has much better software that includes "engine protection". -The overboost protection in the Haltech is now configured and active.....no explanation needed :lol: -Allen thinks that the most likely reason the engine went "boom" was due to extremely conservative timing resulting in high EGTs and ignition of the intake charge. Hence the trip to let the pros tune this time. -The previous gas I was using was Sonocco 116 supplied by a local performance shop. This is one of those deals where it is transferred from a drum to my container. I can't be a hundred percent sure that the guy pumping didn't get things mixed up and give me the wrong gas. So from now on...........C16 from sealed 5 gallon containers, direct from VP. - The CAS is being replaced by a Full Function Trigger wheel with a Hall Effect sensor just in case the CAS signal got a little flakey causing the engine to pop. Anything that is more resistant to noise and gives a more stable timing signal is all good in my book. Should have the necessary parts machined to adapt their kit to my gilmer pulley this week. - EGTs are now being logged in the Haltech. I didn't have this working during the previous dyno runs and might have been able to see that something wasn't quite right prior to the engine letting go. When the engine popped, it was the first run with the EGT's being logged, and by that time, it was too late. -EGTs in the rear rotor were slightly higher than the front, so now I am running 2% more fuel on the rears vs the front to even them out a bit. Let's hope the changes pay off. If they don't.....the new tow hooks will! |
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