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-   -   Is my Apex seal gone? Full story, with afterwards testing done.... (https://www.rx7club.com/3rd-generation-specific-1993-2002-16/my-apex-seal-gone-full-story-afterwards-testing-done-471495/)

BoOsTin FD 10-16-05 10:04 PM

Yeah, the problem was with using the Piston engine compression tool, i wasn't able to see if there are any differences in the spikes on the front rotor.

But when i moved it manually and was listening for the puffs, you can definetelly tell one is the loudest and other 2 are kind of low...

Today, i removed the engine and tomorrow i'm gonna remove everything off of it and get it ready for tear down.

BoOsTin FD 10-25-05 09:40 PM

Well, it turns out 1 apex seal is broken on the front rotor. It also messed up my front housing so i need to start shopping for one.

Just wanted to give a little update.

dubulup 10-26-05 11:07 AM

good luck with the build...careful how hard you push those little hair dryers.

look into WI this build.

BoOsTin FD 10-26-05 11:42 AM

what's a WI?

rfreeman27 10-26-05 12:26 PM

Hate to say I told you so...

allright!


good luck with the build, look into ditching thoes stock Peices of junk.

As dub said water injection would be a good idea to keep that charge air temp in check.

-bobby

BoOsTin FD 10-26-05 03:01 PM

what stock pieces of junk? the twins?

I suspected the seal but i wanted to make sure before i took the engine apart.

What do i need water injection for? I think the intake temps were low enough. I'm still not sure why it blew...

G's 3rd Gen 10-26-05 03:51 PM

could it have been a the primary injector misfiring causing a lean condition? partial clog?

dubulup 10-26-05 04:05 PM


Originally Posted by BoOsTin FD
I think the intake temps were low enough. I'm still not sure why it blew...


SMIC and 15psi on twins = not cool intake temps.

that's my guess why it blew

BoOsTin FD 10-26-05 05:37 PM

It was 50 degrees outside i doubt the smic wasn't cooling it enough. I know when i pulled over, the intake side of the IC was mild not hot or anything.


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